tin removal
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2021 ◽  
Vol 83 (6) ◽  
pp. 1418-1428
Author(s):  
Avery L. Carlson ◽  
Huanqi He ◽  
Cheng Yang ◽  
Glen T. Daigger

Abstract Mathematical modelling was used to investigate the possibility to use membrane aerated biofilm reactors (MABRs) in a largely anoxic suspended growth bioreactor to produce the nitrate-nitrogen required for heterotrophic denitrification and the growth of denitrifying phosphorus accumulating organisms (DPAOs). The results indicate that such a process can be used to achieve a variety of process objectives. The capture of influent biodegradable organic matter while also achieving significant total inorganic nitrogen (TIN) removal can be achieved with or without use of primary treatment by operation at a relatively short suspended growth solids residence time (SRT). Low effluent TIN concentrations can also be achieved, irrespective of the influent wastewater chemical oxygen demand (COD)/total nitrogen (TN) ratio, with somewhat larger suspended growth SRT. Biological phosphorus and nitrogen removal can also be effectively achieved. Further experimental work is needed to confirm these modelling results.


Author(s):  
Y. Feng ◽  
X.-Q. Peng ◽  
H.-H. Shi ◽  
W. Zhang ◽  
Q.-T. Zuo

This paper mainly investigated on synthesis of a high purity PbS crystal directly from lead ash which was collected from Tin ash removal process (LATR). The LATR was firstly disposed by nitric acid leaching system to generate the lead nitrate solution. The PbS crystal would be prepared by mixing the lead nitrate solution with the sodium sulfide at the room temperature (25 ?C). The effects of molar ratio of HNO3 to Pb in the LATR on Pb leaching efficiency was investigated, demonstrating that the Pb leaching efficiency could attain to 82.9 % at molar ratio of 3. The leaching ratio of As, Cu, Fe, and Al generally increased with increasing molar ratio of HNO3 to Pb in the LATR, while 99.99 wt% of Sn was still left in the residue. In the process of generating PbS crystal from the leaching solution, the yield of PbS crystal was increased with increasing molar ratio of Na2S to Pb in the filtrate. The yield of PbS crystal could up to 93.1% at a molar ratio of 1.5. Overall, this method proved to be an efficient and environmental friendly route for synthesis of high quality PbS crystal directly from the common lead containing waste from the lead ore or secondary smelting factory.


2020 ◽  
Vol 42 (12) ◽  
pp. 623-636
Author(s):  
Shinyo Chang ◽  
Pung Shik Shin ◽  
Hyeon Park ◽  
Yeon-Koo Jeong

Objectives:By measuring the solids loading rate for the sidestream, it was intended to achieve increased treatment capacity and improved process performance by developing control technologies for primary sludge removal, recirculation, and input.Methods:The pilot plant was manufactured by the primary clarifier+MLE process similar to the full-scale plant and was configured to control the amount of sludge withdrawal based on the inflow solids loading rate. The state point analysis was used to determine removal underflow withdrawal rate and the total underflow withdrawal rate for the primary sludge. The operation was divided into manual withdrawal, automatic withdrawal, automatic withdrawal+recirculation, and automatic withdrawal + input methods. The performance evaluation items for primary sludge control technology were primary sludge concentration and SS removal efficiency for primary and secondary clarifiers. The improvement in the performance of the bioreactor by recirculation and input was judged through the removal efficiency of ammonium nitrogen, TIN (Total Inorganic Nitrogen) and phosphate phosphorus, SNR (Specific Nitrification Rate), and SDNR (Specific Denitrification Rate). The cause of the performance improvement was analyzed by comparing the acetic acid concentration changed by recirculation and the microbial community characteristics.Results and Discussion:The average value of SS monitoring of the sidestream influent was 2.2 (0.7~6.3) g/L and the primary clarifier needed treatment in response to high concentration SS and fluctuations. It is judged that the state point analysis based on the actual settling rate can accurately suggest whether the stable operation of primary sludge removal, recirculation, and input is the possible and specific design and operation standards. The automatic withdrawal that controls the underflow withdrawal rate according to the change of the inflow solids loading rate could stably draw out the high-concentration sludge and maintain the SS removal efficiency. It is believed that stable operation is possible even in the sludge recirculation operation, and the treatment capacity of the primary clarifier can be increased more than two times in a full-scale plant. By recirculation of the primary sludge, the TIN removal efficiency in the bioreactor was improved by 24.2~52.3%, and the phosphate phosphorus removal efficiency was improved by up to 20.1%. The TIN removal efficiency in the bioreactor was improved by 32.6% by the input of primary sludge. VFAs (Volatile Fatty Acids) including acetic acid was produced and the removal efficiency was improved because it was in contact with primary sludge by recirculation and the ratio of major fermentation microorganisms was present at 2.0%. It is determined that 26.4% of the main species of microorganisms treated with nitrogen and phosphorus exist in the sidestream inflow and the removal efficiency was improved by supplying microorganisms through the input of primary sludge.Conclusions:Technology that controls primary sludge removal, recirculation, and input by measuring the solids loading rate for the sidestream is believed to increase the treatment capacity of the primary clarifier and improve the nitrogen and phosphorus removal efficiency of the bioreactor.


2020 ◽  
Vol 82 (12) ◽  
pp. 2990-3002
Author(s):  
Han Yang ◽  
Liangwei Deng ◽  
Youqian Xiao ◽  
Hongnan Yang ◽  
Hong Wang ◽  
...  

Abstract In this study, the performance and mechanism of nitrogen removal in sequencing batch reactors (SBRs) with and without zero-valent iron (ZVI) was investigated. The results showed that ZVI had a capacity to promote -N conversion, -N accumulation and total inorganic nitrogen (TIN) removal, with the TIN removal rate being increased by 29.45%. The ZVI also had a significant impact on microbial community structure by means of high-throughput pyrosequencing, increasing the enrichment of Anammox (anaerobic ammonium oxidation) bacteria Candidatus Brocadia and Feammox (anaerobic ferric ammonium oxidation) bacteria Ignavibacterium. With ZVI addition, the main pathway of nitrogen removal was changed from nitrification-heterotrophic denitrification to Anammox and Feammox.


2020 ◽  
Vol 16 ◽  
pp. 102862
Author(s):  
Xiang Zhang ◽  
Guojun Ma ◽  
Mengke Liu ◽  
Zhi Li ◽  
Mingming Song

2020 ◽  
Vol 6 (12) ◽  
pp. 3415-3427
Author(s):  
Paul Roots ◽  
Alex F. Rosenthal ◽  
Quan Yuan ◽  
Yubo Wang ◽  
Fenghua Yang ◽  
...  

Mainstream deammonification performance in an integrated fixed film activated sludge (IFAS) reactor improved from 46% to 73% TIN removal after routing 10% of the primary effluent around the A-stage reactor.


2019 ◽  
Vol 15 (2) ◽  
pp. 87-91
Author(s):  
Rabin Maharjan ◽  
Iswar Man Amatya ◽  
Ram Kumar Sharma

Use of ground water containing ammonical nitrogen has been increasing in Kathmandu valley. The use of locally and cheaply fitted Hydrogenotrophic Denitrification (HD) has been taken as an effective way to remove the nitrates in this study. Comparative analysis of HD reactors had been studied for the determination of the effective flow direction of water as Up Flow or Down Flow. The result reviled that flow direction as Down Flow HD reactor performed slightly better than Up Flow HD reactor. The maximum NO3-N conversion reached 100% for Down Flow and 98.65% for Up Flow reactor with maximum of total inorganic nitrogen (TIN) removed were 41.11% and 33.89% for Down Flow and Up Flow reactor respectively. The difference in NO3-N conversion and TIN removal were observed. As the NO2-N was accumulated, suggesting NO3 conversion is higher than NO2 conversion thus, and majorly incomplete denitrification existed. The NO2-N in water reached to maximum of 78.89 mg/l and 72.55 mg/l for Down Flow and Up Flow rector.


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