scholarly journals Aerobic sequencing batch reactor for the treatment of industrial wastewater from the brewery

2017 ◽  
Author(s):  
◽  
Khaya Pearlman Shabangu

One of the major effects of socio-economic change due to industrialisation is the generation of industrial wastewater, which requires treatment before being released into the environment. Laboratory-scale aerobic sequencing batch reactors under suspended-growth heterotrophic activated sludge were operated in different aeration configurations to study their effect on the treatment of wastewater generated by a local brewery. The main purpose of this study was to evaluate the performance of the two laboratory-scale aerobic sequencing batch reactors treating brewery wastewater under continuous low-oxygen dosing concentration and cyclic aeration schemes on SBR operation. The characterisation of brewery wastewater was undertaken to assess the physicochemical composition of the wastewater produced from one of the breweries in South Africa (SAB). The data showed distinctive characteristics of brewery wastewater, which coincided with studies previously carried out on characterisation of brewery wastewater. The COD average concentration of the brewery influent was 7100 mg/L, with average pH values of 7. The BOD and the total solids content of the brewery wastewater influent from the facility were both high, implying that the influent was very rich in organic content and its discharge into water-receiving bodies or the municipal treatment plant could have adverse effects. From these results, a need for a competitive treatment technology was clearly highlighted so as to carry out a feasible treatment of the influent for the brewery industry. The aerobic sequencing batch reactors were designed, fabricated and set up for laboratory-scale treatment of wastewater from the brewery for 15 weeks. The performance of the two SBR configurations was determined with reference to COD, BOD, TS, VS and TSS. The experimental results demonstrated that wastewater generated from the breweries can be treated successfully using both aeration configurations. The results obtained indicated that treatment efficiencies in terms of COD and BOD were 94 % and 85 % respectively, for the reactor operated under continuous aeration configuration, while 81 % and 65 % was achieved for the reactor operated in the cyclic aeration scheme. The findings from this study demonstrate that the performance of the reactor operated under the continuous aeration scheme was successful, and showed statistically significant differences from the performance of the reactor operated under cyclic aeration schemes. These findings imply that there is a potential for the equipment, including financial benefit as a result of operating aerobic sequencing batch reactors for treating brewery wastewater under continuous low-oxygen concentration dosing schemes. In this study, it was also established that the maximum COD removal could be reached at an optimum hydraulic retention times of 5 days for both reactors. This was based upon viewing the experimental data; it appeared that the most significant difference in percentage COD removal was for HRTs 3 days and 4 days. Although, due to less percentage COD removal observed from HRTs 5 days till 7 days, it was hence established that the optimum removal of high strength organics in the brewery wastewater could be achieved within 5 days of treatment time. The pH adapted at an average of 7 for all batch experimentations of the study. The temperature maintained an average of 23 oC ambient, throughout the experimental period. These physical parameters ensured that the microbial population was kept healthy, without inhibiting its biological degradation activity. Although, sludge build up was observed in both aerobic SBRs on completion of each batch operation due to solids retention and organic pollutants biodegradation from the brewery wastewater. It was perceived that frequently reseeding both aerobic SBRs, as an alternative to 28 days sludge retention time would enhance the recovery of biomass, thus improving the overall removal of TSS consequently minimising sludge bulking in both reactors.

1999 ◽  
Vol 39 (6) ◽  
pp. 61-68 ◽  
Author(s):  
Klangduen Pochana ◽  
Jürg Keller

Experiments have been performed to gain an understanding of the conditions and processes governing the occurrence of SND in activated sludge systems. Sequencing batch reactors (SBRs) have been operated under controlled conditions using the wastewater from the first anaerobic pond in an abattoir wastewater treatment plant. Under specific circumstances, up to 95% of total nitrogen removal through SND has been found in the system. Carbon source and oxygen concentrations were found to be important process parameters. The addition of acetate as an external carbon source resulted in a significant increase of SND activity in the system. Stepwise change of DO concentration has also been observed in this study. Experiments to determine the effect of the floc size on SND have been performed in order to test the hypothesis that SND is a physical phenomenon, governed by the diffusion of oxygen into the activated sludge flocs. Initial results support this hypothesis but further experimental confirmation is still required.


2016 ◽  
Vol 2016 ◽  
pp. 1-8
Author(s):  
Dong-sheng Shen ◽  
Li-jia Wang ◽  
Hong-zhen He ◽  
Mei-zhen Wang

Bioaugmentation with degrading bacteria can improve the treatment of nicotine-containing tobacco industrial wastewater effectively. However, the transient and extremely high feeding of pollutants may compromise the effectiveness of the bioaugmented reactors. The effect of transient nicotine shock loads on the performance ofPseudomonassp. HF-1 bioaugmented SBRs were studied. The results showed that, under 500–2500 mg/L of transient nicotine shocks, all the reactors still could realize 100% of nicotine degradation in 4 days of recovery, while the key nicotine degradation enzyme HSP hydroxylase increased in expression. Though the dramatic increase of activities of ROS, MDA, SOD, and CAT suggested that transient nicotine shock loads could induce oxidative stress on microorganisms in activated sludge, a decrease to control level demonstrated that most of the microorganisms could resist 500–1500 mg/L of transient nicotine shock under the protection from strain HF-1. After 8 cycles of recovery, high ROS level and low TOC removal in high transient shock reactors implied that 2000–2500 mg/L of transient nicotine shock was out of its recovery of strain HF-1 bioaugmented system. This study enriched our understanding on highly efficient nicotine-degrading strain bioaugmented system, which would be beneficial to tobacco waste or wastewater treatment in engineering.


2018 ◽  
Author(s):  
◽  
Siphesihle Mangena Khumalo

South Africa is not an exception when it comes to the issue of fresh water scarcity perpetuated by environmental pollution among many other factors. Industrial wastewater particularly emanating from the brewing industry, contains high-strength organic, inorganic, and biological compounds which are toxic to the environment. Due to stringent industrial effluent dewatering standards enforced by both local and international environmental protection entities, industrial wastewater cannot be discharged into receiving water bodies prior to treatment. The overall aim of this study was to evaluate the performance or treatment efficacy of a laboratory scale sequencing batch reactor on biological nutrient removal using industrial wastewater from brewery. In this study, two laboratory scale sequencing batch reactors (SBRs) operated in a cyclic aerobic-anaerobic configuration inoculated with activated sludge were investigated for their removal of orthophosphates and nitrogen compounds from brewery wastewater. SBR-1 was investigated for nitrogen group pollutant removal and SBR-2 was investigated for orthophosphate removal. The findings of the study are reported based on overall removal efficacies for the following process monitoring parameters: orthophosphates, ammoniacal nitrogen, total Kjeldahl nitrogen, total nitrogen, total organic nitrogen, total inorganic nitrogen and NO3-N+NO2-N. From the investigation, the following overall removal efficacies were obtained: 69% orthophosphates, 69% ammoniacal nitrogen, 59% total Kjeldahl nitrogen, 60% total nitrogen, 64% total organic nitrogen, 67% total inorganic nitrogen and 56% NO3-N+NO2-N at an organic loading rate of 3.17 kg Total Chemical Oxygen Demand (TCOD) /m3.day with a food to microorganism ratio of 2.86 g TCOD/g Volatile Suspended Solids (VSS).day. These removal efficacies were attained for a hydraulic retention time of 18 hours for both SBRs with a solids retention time of 5 days for SBR-1 and 7 days for SBR-2. Both reactors were operated at a mesophilic temperature range of 23 to 26˚C and a pH range of 5 to 8.5. The temperature was left unadjusted because it was observed that it did not hinder any microbial activities during the biodegradation process. The Michealis-Menten’s and Monod models were implemented to study the substrate utilisation rate kinetics and microbial growth rate kinetics recording 15 141 g COD/m3.day; 12 518 g VSS/g VSS.day; 20 343 g COD/m3.day and 16 860 g VSS/g VSS.day for SBR-1 and SBR-2, respectively. The Monod model demonstrated a strong correlation fit between the substrate utilisation rate and microbial growth rate recording a polynomial correlation constant of R2 = 0.947 and 0.9582 for SBR-1 and SBR-2, respectively. The findings of this study showed that the cyclic aerobic-anaerobic configuration on a laboratory scale SBR inoculated with activated sludge for treatment of brewery wastewater for biological nutrients was feasible.


2020 ◽  
Vol 8 (5) ◽  
pp. 716
Author(s):  
Xueling Wu ◽  
Han Zhou ◽  
Liangzhi Li ◽  
Enhui Wang ◽  
Xiangyu Zhou ◽  
...  

Halotolerant microorganisms are promising in bio-treatment of hypersaline industrial wastewater. Four halotolerant bacteria strains were isolated from wastewater treatment plant, of which a strain LZH-9 could grow in the presence of up to 14% (w/v) NaCl, and it removed 81.9% chemical oxygen demand (COD) at 96 h after optimization. Whole genome sequencing of Lysinibacillus pakistanensis LZH-9 and comparative genomic analysis revealed metabolic versatility of different species of Lysinibacillus, and abundant genes involved in xenobiotics biodegradation, resistance to toxic compound, and salinity were found in all tested species of Lysinibacillus, in which Horizontal Gene Transfer (HGT) contributed to the acquisition of many important properties of Lysinibacillus spp. such as toxic compound resistance and osmotic stress resistance as revealed by phylogenetic analyses. Besides, genome wide positive selection analyses revealed seven genes that contained adaptive mutations in Lysinibacillus spp., most of which were multifunctional. Further expression assessment with Codon Adaption Index (CAI) also reflected the high metabolic rate of L. pakistanensis to digest potential carbon or nitrogen sources in organic contaminants, which was closely linked with efficient COD removal ability of strain LZH-9. The high COD removal efficiency and halotolerance as well as genomic evidences suggested that L. pakistanensis LZH-9 was promising in treating hypersaline industrial wastewater.


2012 ◽  
Vol 610-613 ◽  
pp. 2068-2073
Author(s):  
Ya Jing Li ◽  
Li Ping Sun ◽  
Min Ji

The nitrogen and phosphorus removal efficiency and effect of different electron acceptors (O2 and NO3-) on the sludge yield were studied through experiments in two SBRs (Sequencing Batch Reactors ) in this paper. The results showed that two systems both had good decontamination effect; the theory value of sludge yield (It was 0.435gVSS/gCOD and 0.402gVSS/gCOD for anaerobic /aerobic and anaerobic/anoxic condition, respectively) was higher than the actual value (It was 0.335gVSS/gCOD and 0.321g VSS/gCOD for anaerobic/aerobic and anaerobic/anoxic condition, respectively); There was no significant difference for the sludge yield under anaerobic/aerobic and anaerobic/anoxic conditions, because the endogenesis respiration of sludge under anaerobic/aerobic condition was stronger consequently more sludge being attenuated (Attenuation coefficient was 0.0081 and 0.0026 for anaerobic/aerobic and anaerobic/anoxic condition, respectively).


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