scholarly journals The influence of dissolved oxygen on partial nitritation/anammox performance and microbial community of the 200,000 m3/d activated sludge process at the Changi water reclamation plant (2011 to 2016)

2018 ◽  
Vol 78 (3) ◽  
pp. 634-643 ◽  
Author(s):  
Yeshi Cao ◽  
Bee Hong Kwok ◽  
Mark C. M. van Loosdrecht ◽  
Glen Daigger ◽  
Hui Yi Png ◽  
...  

Abstract Mainstream partial nitritation/anammox (PN/A), coupled with excess biological phosphorus removal, in a 200,000 m3/d step-feed activated sludge process (Train 2) in the Changi Water Reclamation Plant (WRP), Singapore, has been studied and reported. This paper presents an overview of process performance and the microbial community during the period from 2011 to 2016. The site data showed that, along with the reduction of dissolved oxygen (DO) from 1.7 to 1.0 mg O2/L in the aeration zones, the concentrations of ammonium and nitrate of the final effluent increased, while nitrite decreased, resulting in an increase of 2.4 mg N/L of total inorganic nitrogen. Autotrophic nitrogen removal was higher than heterotrophic biological nitrogen removal under higher DO concentration conditions, but decreased under low DO operating condition. These macro-scale changes were caused by shifts of the nitrogen-converting microbial community. The ammonia oxidizing bacteria (AOB) population abundance was reduced by 30 times, while the nitrite oxidizing bacteria (NOB) population abundance and specific activity increased significantly with a shift of dominant genus from Nitrobacter to Nitrospira. The ratio of AOB and NOB specific activities were reduced from 12.8 to 1.6, and the ex situ nitrite accumulation ratio reduced from 76% to 29%. Changes in the microbial community and overall process performance illustrated that, compared to the excellent NOB suppression under high DO conditions, NOB were more active after the DO concentration reduction despite still being partly suppressed. This case study demonstrated, for the first time, the influence of DO reduction on the nitrogen conversion microbial community and PN/A process performance for a suspended growth system. Its relevance to biofilm and hybrid PN/A processes is also discussed.

2020 ◽  
Vol 81 (2) ◽  
pp. 333-344
Author(s):  
Jianfeng Wen ◽  
Mark W. LeChevallier ◽  
Wendong Tao

Abstract Simultaneous nitrification and denitrification under low dissolved oxygen conditions is an energy-saving modification of the activated sludge process to achieve efficient nitrogen removal. Geographically distinct full-scale treatment plants are excellent platforms to address the links of microbial community with operating parameters. Mixed liquor samples were collected from a sequencing batch reactor plant, oxidation ditch plant, and step-feed activated sludge plant. Next-Generation Sequencing of the samples showed that the microbial communities were similar at the phylum level among the plants, being dominated by Proteobacteria. Microbial composition of functional groups was similar between the react fill and react phases of the sequencing batch reactors, among four sequencing batch reactors, and among four oxidation ditches. Nitrospira was the only identified genus of autotropic nitrifying bacteria with a relative abundance of 2.2–2.5% in the oxidation ditches and 0.4–0.7% at the other plants. Heterotrophic nitrifying–aerobic denitrifying bacteria were dominated by Dechloromonas with a relative abundance of 0.4–1.0%. Microbial community composition and nitrogen removal mechanisms were related to overall level and local zonation of dissolved oxygen, mixed liquor suspended solids concentration, nitrogen and organic loadings, and solids retention time. Low dissolved oxygen and low organic and nitrogen loadings favored growth of Nitrospira.


2016 ◽  
Vol 75 (3) ◽  
pp. 741-751 ◽  
Author(s):  
Yeshi Cao ◽  
Bee Hong Kwok ◽  
Mark C. M. van Loosdrecht ◽  
Glen T. Daigger ◽  
Hui Yi Png ◽  
...  

Mainstream partial nitritation and Anammox (PN/A) has been observed and studied in the step-feed activated sludge process at the Changi water reclamation plant (WRP), which is the largest WRP (800,000 m3/d) in Singapore. This paper presents the study results for enhanced biological phosphorus removal (EBPR) co-existing with PN/A in the activated sludge process. Both the in-situ EBPR efficiency and ex-situ activities of phosphorus release and uptake were high. The phosphorus accumulating organisms were dominant, with little presence of glycogen accumulating organisms in the activated sludge. Chemical oxygen demand (COD) mass balance illustrated that the carbon usage for EBPR was the same as that for heterotrophic denitrification, owing to autotrophic PN/A conversions. This much lower carbon demand for nitrogen removal, compared to conventional biological nitrogen removal, made effective EBPR possible. This paper demonstrated for the first time the effective EBPR co-existence with PN/A in the mainstream in a large full-scale activated sludge process, and the feasibility to accommodate EBPR into the mainstream PN/A process. It also shows EBPR can work under warm climates.


2011 ◽  
Vol 64 (5) ◽  
pp. 1009-1015 ◽  
Author(s):  
G. Cema ◽  
E. Płaza ◽  
J. Trela ◽  
J. Surmacz-Górska

A biofilm system with Kaldnes biofilm carrier was used in these studies to cultivate bacteria responsible for both partial nitritation and Anammox processes. Due to co-existence of oxygen and oxygen-free zones within the biofilm depth, both processes can occur in a single reactor. Oxygen that inhibits the Anammox process is consumed in the outer layer of the biofilm and in this way Anammox bacteria are protected from oxygen. The impact of oxygen concentration on nitrogen removal rates was investigated in the pilot plant (2.1 m3), supplied with reject water from the Himmerfjärden Waste Water Treatment Plant. The results of batch tests showed that the highest nitrogen removal rates were obtained for a dissolved oxygen (DO) concentration around 3 g O2 m−3. At a DO concentration of 4 g O2 m−3, an increase of nitrite and nitrate nitrogen concentrations in the batch reactor were observed. The average nitrogen removal rate in the pilot plant during a whole operating period oscillated around 1.3 g N m−2d−1 (0.3 ± 0.1 kg N m−3d−1) at the average dissolved oxygen concentration of 2.3 g O2 m−3. The maximum value of a nitrogen removal rate amounted to 1.9 g N m−2d−1 (0.47 kg N m−3d−1) and was observed for a DO concentration equal to 2.5 g O2 m−3. It was observed that increase of biofilm thickness during the operational period, had no influence on nitrogen removal rates in the pilot plant.


2020 ◽  
Vol 53 (5) ◽  
pp. 671-679
Author(s):  
Abdallah Lemita ◽  
Sebti Boulahbel ◽  
Sami Kahla ◽  
Moussa Sedraoui

Dissolved oxygen (DO) concentration is a key variable in the activated sludge wastewater treatment processes. In this paper, an auto control strategy based on Euler method and gradient method with radial basis function (RBF) neural networks (NNs) is proposed to solve the DO concentration control problem in an activated sludge process of wastewater treatment. The control purpose is to maintain the dissolved oxygen concentration in the aerated tank for having the substrate concentration within the standard limits established by legislation of wastewater treatment. For that reason, a new proposed control strategy based on gradient descent method and RBF neural network has been used. Compared with RBF neural network PI control, the obtained results show the effectiveness in terms of both transient and steady performances of proposed control method for dissolved oxygen control in the activated sludge wastewater treatment processes.


1992 ◽  
Vol 25 (4-5) ◽  
pp. 203-209 ◽  
Author(s):  
R. Kayser ◽  
G. Stobbe ◽  
M. Werner

At Wolfsburg for a load of 100,000 p.e., the step-feed activated sludge process for nitrogen removal is successfully in operation. Due to the high denitrification potential (BOD:TKN = 5:1) the effluent total nitrogen content can be kept below 10 mg l−1 N; furthermore by some enhanced biological phosphate removal about 80% phosphorus may be removed without any chemicals.


1996 ◽  
Vol 33 (12) ◽  
pp. 243-250 ◽  
Author(s):  
O. Nowak ◽  
A. Franz ◽  
K. Svardal ◽  
V. Müller

By means of theoretical considerations and of statistical evaluations, specific organic and nitrogen loads in separately stabilized sludge have been found to be in the range of 16 to 20g VSS/PE/d and of 1.1 to 1.5 g N/PE/d respectively. About 0.6g P/PE/d are removed from the wastewater in activated sludge plants without chemical or enhanced biological P removal. By using the single-stage activated sludge process without primary sedimentation and without separate sludge stabilization, almost complete nitrogen removal can be achieved, but specific organic and nitrogen loads in the waste sludge are up to two times higher than in separately stabilized sludge.


2020 ◽  
Vol 148 ◽  
pp. 01002
Author(s):  
Herto Dwi Ariesyady ◽  
Mentari Rizki Mayanda ◽  
Tsukasa Ito

Activated sludge process is one of the wastewater treatment method that is applied for many wastewater types including painting process wastewater of automotive industry. This wastewater is well-known to have high heavy metals concentration which could deteriorate water environment if appropriate performance of the wastewater treatment could not be achieved. In this study, we monitored microbial community diversity in a Painting Biological Treatment (PBT) system. We applied a combination of cultivation and genotypic biological methods based on 16S rRNA gene sequence analysis to identify the diversity of active microbial community. The results showed that active microbes that could grow in this activated sludge system were dominated by Gram-negative bacteria. Based on 16S rRNA gene sequencing analysis, it was revealed that their microbial diversity has close association with Bacterium strain E286, Isosphaera pallida, Lycinibacillus fusiformis, Microbacterium sp., Orchobactrum sp., Pseudomonas guariconensis, Pseudomonas sp. strain MR84, Pseudomonas sp. MC 54, Serpens sp., Stenotrophomonas acidaminiphila, and Xylella fastidiosa with similarity of 86 – 99%. This findings reflects that microbial community in a Painting Biological Treatment (PBT) system using activated sludge process could adapt with xenobiotics in the wastewater and has a wide range of diversity indicating a complex metabolism mechanism in the treatment process.


2017 ◽  
Vol 41 (2) ◽  
pp. 237-247 ◽  
Author(s):  
Paul Moretti ◽  
Jean-Marc Choubert ◽  
Jean-Pierre Canler ◽  
Pierre Buffière ◽  
Olivier Pétrimaux ◽  
...  

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