Early in situ measurement of radioactive fallout in Fukushima city due to Fukushima Daiichi nuclear accident

2012 ◽  
Vol 155 (2) ◽  
pp. 181-196 ◽  
Author(s):  
M. Takada ◽  
T. Suzuki
2015 ◽  
Vol 68 ◽  
pp. 616-626 ◽  
Author(s):  
Naofumi Kozai ◽  
Shinichi Suzuki ◽  
Noboru Aoyagi ◽  
Fuminori Sakamoto ◽  
Toshihiko Ohnuki

2013 ◽  
Vol 58 (1) ◽  
pp. 283-290 ◽  
Author(s):  
Y. Nishizaki ◽  
H. Miyamae ◽  
S. Ichikawa ◽  
K. Izumiya ◽  
T. Takano ◽  
...  

Our effort for decontamination of radioactive cesium scattered widely by nuclear accident in March 2011 in Fukushima, Japan has been described. Radioactive cesium scattered widely in Japan has been accumulating in arc or plasma molten-solidified ash in waste incinerating facilities up to 90,000 Bq/kg of the radioactive waste. Water rinsing of the ash resulted in dissolution of cesium ions together with high concentrations of potassium and sodium ions. Although potassium inhibits the adsorption of cesium on zeolite, we succeeded to precipitate cesium by in-situ formation of ferric ferrocyanide and iron rust in the radioactive filtrate after rinsing of the radioactive ash with water. Because the regulation of no preservation of any kind of cyanide substances, cesium was separated from the precipitate consisting of cesium-captured ferric ferrocyanide and ferric hydroxide in diluted NaOH solution and subsequent filtration gave rise to the potassium-free radioactive filtrate. Cesium was captured by zeolite from the potassium-free radioactive filtrate. The amount of this final radioactive waste of zeolite was significantly lower than that of the arc-molten-solidified ash.


2003 ◽  
Vol 2 (4) ◽  
pp. 589
Author(s):  
Douglas R. Cobos ◽  
John M. Baker

2015 ◽  
Vol 84 (8) ◽  
pp. 567-572
Author(s):  
Tadafumi HASHIMOTO ◽  
Masahito MOCHIZUKI

Author(s):  
Philipp Peter Breese ◽  
Tobias Hauser ◽  
Daniel Regulin ◽  
Stefan Seebauer ◽  
Christian Rupprecht

AbstractThe powder mass flow rate is one of the main parameters regarding the geometrical precision of built components in the additive manufacturing process of laser metal deposition. However, its accuracy, constancy, and repeatability over the course of the running process is not given. Reasons among others are the performance of the powder conveyors, the complex nature of the powder behavior, and the resulting issues with existing closed-loop control approaches. Additionally, a direct in situ measurement of the powder mass flow rate is only possible with intrusive methods. This publication introduces a novel approach to measure the current powder mass flow rate at a frequency of 125 Hz. The volumetric powder flow evaluation given by a simple optical sensor concept was transferred to a mass flow rate through mathematical dependencies. They were found experimentally for a nickel-based powder (Inconel 625) and are valid for a wide range of mass flow rates. With this, the dynamic behavior of a vibration powder feeder was investigated and a memory effect dependent on previous powder feeder speeds was discovered. Next, a closed-loop control with the received sensor signal was implemented. The concept as a whole gives a repeatable and accurate powder mass flow rate while being universally retrofittable and applicable. In a final step, the improved dynamic and steady performance of the powder mass flow rate with closed-loop control was validated. It showed a reduction of mean relative errors for step responses of up to 81% compared to the uncontrolled cases.


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