Dynamic Simulations of New Well Control Procedures Used to Prepare a Dual Gradient System Field Trial

Author(s):  
J. H. Cohen ◽  
R. Stave ◽  
E. Hauge ◽  
J. M. Godhavn ◽  
D. O. Molde
2006 ◽  
Vol 21 (04) ◽  
pp. 287-295 ◽  
Author(s):  
Jerome J. Schubert ◽  
Hans C. Juvkam-Wold ◽  
Jonggeun Choe

2015 ◽  
Author(s):  
E. Hauge ◽  
J.M. Godhavn ◽  
D.O. Molde ◽  
J.H Cohen ◽  
R.S. Stave ◽  
...  

2015 ◽  
Author(s):  
John H. Cohen ◽  
Roger Stave ◽  
Espen Hauge ◽  
Dag Ove Molde

1985 ◽  
Vol 1985 (1) ◽  
pp. 311-313 ◽  
Author(s):  
S. D. Gill ◽  
C. A. Bonke ◽  
J. Carter

ABSTRACT During the evening of February 22, 1984, the Uniacke G-72 gas well being drilled 150 nautical miles off Halifax, Nova Scotia, by the semisubmersible drilling rig, Vinland, under contract to Shell Canada Resources, blew out of control, emitting gas and condensate at an estimated rate of 300 bbl per day. During the following 10 days while Shell was assembling personnel, vessels, and equipment for reboarding the rig and initiating well control procedures, a comprehensive environmental monitoring program was put in place. An air, slick, and water column sampling program was initiated to provide information on the physical and chemical properties of the condensate. This paper describes the primary findings of the program that involved the coordination of government, area petroleum operators, and consultants.


2005 ◽  
Author(s):  
R. Stave ◽  
R. Farestveit ◽  
S. Høyland ◽  
P.O. Rochmann ◽  
N.L. Rolland

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