Reduce odor and NH3 emission: condensation of the carbonatation vapors

2017 ◽  
pp. 534-537
Author(s):  
Nico Antens ◽  
Jan L.M. Struijs

At beet sugar production, vapors from first and second carbonatation contain a significant amount of odor components, NH3 and waste heat, which are normally directly released into the environment. Due to sustainability motivations, obligations regarding odor nuisance and expected stricter regulations regarding NH3 emission limits, Suiker Unie decided to take measures to reduce emission via the carbonatation vapors. During the 2015 beet campaign, pilot scale plant trials have been performed to investigate the effectiveness of indirect contact and direct contact condensation of these vapors. Based on this experimental work a two-stage gas scrubbing concept was designed: in the first stage main goal is condensing the vapors and reuse the heat of condensation to heat up limed juice, while the actual scrubbing takes place in the second scrubber. This two-stage gas scrubbing installation has been built at the Vierverlaten factory and was started up in the 2016 beet campaign. The background, pilot scale trials, concept of design and achieved reductions in odor and NH3 emission at industrial scale are discussed.

Author(s):  
Shigebumi Aoki ◽  
Akira Inoue ◽  
Yoshiyuki Kozawa ◽  
H. Akimoto

2000 ◽  
Vol 41 (1) ◽  
pp. 163-166 ◽  
Author(s):  
W. Gebert ◽  
P.A. Wilderer

The investigated effects of heating the filling material in trickling filters were carried out at the Ingolstadt wastewater treatment plant, Germany. Two pilot scale trickling filters were set up. Heat exchanger pipings were embedded in the filter media of one of these trickling filters, and the temperature in the trickling filter was raised. The other trickling filter was operated under normal temperature conditions, and was used as a control. The results clearly demonstrate that the performance of trickling filters cannot be constantly improved by heating the biofilm support media. A sustained increase of the metabolic rates did not occur. The decrease of the solubility of oxgen in water and mass transfer limitations caused by an increase of the biofilm thickness are the main reasons for that. Thus, the heating of trickling filters (e.g. by waste heat utilization) in order to increase the capacity of trickling filters under cold weather conditions cannot be recommended.


2021 ◽  
Vol 13 (3) ◽  
pp. 1109
Author(s):  
Edgar Ricardo Oviedo-Ocaña ◽  
Angélica María Hernández-Gómez ◽  
Marcos Ríos ◽  
Anauribeth Portela ◽  
Viviana Sánchez-Torres ◽  
...  

The composting of green waste (GW) proceeds slowly due to the presence of slowly degradable compounds in that substrate. The introduction of amendments and bulking materials can improve organic matter degradation and end-product quality. However, additional strategies such as two-stage composting, can deal with the slow degradation of green waste. This paper evaluates the effect of two-stage composting on the process and end-product quality of the co-composting of green waste and food waste amended with sawdust and phosphate rock. A pilot-scale study was developed using two treatments (in triplicate each), one being a two-stage composting and the other being a traditional composting. The two treatments used the same mixture (wet weight): 46% green waste, 19% unprocessed food waste, 18% processed food waste, 13% sawdust, and 4% phosphate rock. The traditional composting observed a higher degradation rate of organic matter during the mesophilic and thermophilic phases and observed thermophilic temperatures were maintained for longer periods during these two phases compared to two-stage composting (i.e., six days). Nonetheless, during the cooling and maturation phases, the two treatments had similar behaviors with regard to temperature, pH, and electrical conductivity, and the end-products resulting from both treatments did not statistically differ. Therefore, from this study, it is concluded that other additional complementary strategies must be evaluated to further improve GW composting.


2021 ◽  
Vol 39 ◽  
pp. 101873
Author(s):  
Qiming Guo ◽  
Zhihong Yang ◽  
Qun Zhao ◽  
Jing Chen ◽  
Jie Li ◽  
...  
Keyword(s):  

Author(s):  
David Heinze ◽  
Thomas Schulenberg ◽  
Lars Behnke

A simulation model for the direct contact condensation of steam in subcooled water is presented that allows determination of major parameters of the process, such as the jet penetration length. Entrainment of water by the steam jet is modeled based on the Kelvin–Helmholtz and Rayleigh–Taylor instability theories. Primary atomization due to acceleration of interfacial waves and secondary atomization due to aerodynamic forces account for the initial size of entrained droplets. The resulting steam-water two-phase flow is simulated based on a one-dimensional two-fluid model. An interfacial area transport equation is used to track changes of the interfacial area density due to droplet entrainment and steam condensation. Interfacial heat and mass transfer rates during condensation are calculated using the two-resistance model. The resulting two-phase flow equations constitute a system of ordinary differential equations, which is solved by means of the explicit Runge–Kutta–Fehlberg algorithm. The simulation results are in good qualitative agreement with published experimental data over a wide range of pool temperatures and mass flow rates.


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