Anaerobic digestion potential for ecological and decentralised sanitation in urban areas

2006 ◽  
Vol 53 (9) ◽  
pp. 45-54 ◽  
Author(s):  
Tarek Elmitwalli ◽  
Yucheng Feng ◽  
Joachim Behrendt ◽  
Ralf Otterpohl

The potential of anaerobic digestion in ecological and decentralised sanitation has been investigated in this research. Different anaerobic digestion systems were proposed for the treatment of sewage, grey water, black water and faeces. Moreover, mathematical models based on anaerobic digestion model no.1 (ADM1) were developed for determination of a suitable design for each system. For stable performance of an upflow anaerobic sludge blanket (UASB) reactor treating sewage, the model results indicated that optimisation of wastewater conversion to biogas (not COD removal) should be selected for determination of the hydraulic retention time (HRT) of the reactor. For the treatment of sewage or black water in a UASB septic-tank, the model results showed that the sludge removal period was the main parameter for determination of the HRT. At such HRT, both COD removal and wastewater conversion are also optimised. The model results demonstrated that for treatment of faeces in an accumulation (AC) system at temperature ≥25 °C, the filling period of the system should be higher than 60 days. For maximisation of the net biogas production (i.e. reduction of biogas losses as dissolved in the effluent), the separation between grey water, urine and faeces and reduction of water consumption for faeces flushing are required. Furthermore, the faeces and kitchen organic wastes and grey water are digested in, respectively, an AC system and UASB reactor, while the urine is stored.

2011 ◽  
Vol 64 (3) ◽  
pp. 610-617 ◽  
Author(s):  
Tarek Elmitwalli ◽  
Ralf Otterpohl

The treatment of grey water in two upflow anaerobic sludge blanket (UASB) reactors, operated at different hydraulic retention times (HRTs) and temperatures, was investigated. The first reactor (UASB-A) was operated at ambient temperature (14–25 °C) and HRT of 20, 12 and 8 h, while the second reactor (UASB-30) was operated at controlled temperature of 30 °C and HRT of 16, 10 and 6 h. The two reactors were fed with grey water from ‘Flintenbreite’ settlement in Luebeck, Germany. When the grey water was treated in the UASB reactor at 30 °C, total chemical oxygen demand (CODt) removal of 52–64% was achieved at HRT between 6 and 16 h, while at lower temperature lower removal (31–41%) was obtained at HRT between 8 and 20 h. Total nitrogen and phosphorous removal in the UASB reactors were limited (22–36 and 10–24%, respectively) at all operational conditions. The results showed that at increasing temperature or decreasing HRT of the reactors, maximum specific methanogenic activity of the sludge in the reactors improved. As the UASB reactor showed a significantly higher COD removal (31–64%) than the septic tank (11–14%) even at low temperature, it is recommended to use UASB reactor instead of septic tank (the most common system) for grey water pre-treatment. Based on the achieved results and due to high peak flow factor, a HRT between 8 and 12 h can be considered the suitable HRT for the UASB reactor treating grey water at temperature 20–30 °C, while a HRT of 12–24 h can be applied at temperature lower than 20 °C.


2004 ◽  
Vol 31 (3) ◽  
pp. 420-431 ◽  
Author(s):  
S K Patidar ◽  
Vinod Tare

The effect of micro-nutrients, such as Fe, Ni, Zn, Co, and Mo, on anaerobic degradation of sulfate laden organics was investigated using bench-scale models of upflow anaerobic sludge blanket (UASB) reactor, anaerobic baffled reactor (ABR), and hybrid anaerobic baffled reactor (HABR), operating in varying conditions in ten phases (organic loading of 1.9–5.75 kg COD/(m3·d), sulfate loading of 0.54–1.88 kg SO42–/(m3·d), chemical oxygen demand (COD):SO42–ratio of 2.0–8.6). In the initial phase, no nutrient limitation was observed with COD removal of more than 94% in all three systems. Subsequently, increase in sulfate loading resulted in Ni and Co limitation and their supplementation restored COD removal in UASB system. However, baffled systems did not recover because of severe inhibition by sulfide. Results indicate that precipitation of nutrients could seriously deteriorate process performance, leading to failure even before sulfide concentration attains toxic level. The limitation of Fe coupled with high sulfate loading (1.88 kg SO42–/(m3·d)) resulted in growth of low-density, fragile, hollow, and granular biomass in UASB that washed out and caused process instability. Supplementation of Fe with other nutrients stabilized UASB process and also improved COD removal.Key words: anaerobic degradation, nutrients, UASB, ABR, HABR, sulfide toxicity, sulfate laden organics.


2018 ◽  
Vol 78 (9) ◽  
pp. 1871-1878 ◽  
Author(s):  
Gustavo Vargas-Morales ◽  
Rolando Chamy ◽  
Santiago García-Gen

Abstract A variable-gain controller for anaerobic digestion of industrial winery wastewater is presented. A control law using both volatile fatty acids (VFA) and methane production rate as controlled variables and organic loading rate (OLR) as manipulated variable is defined. The process state is quantitatively estimated by an empirical function comparing VFA measurements against a setpoint value; then, it is modified with a second empirical function that compares the methane flow rate with a maximum capacity reference, and finally it is adjusted with a third factor considering the actual hydraulic retention time. The variable-gain function determines the extent of the OLR change applied to the system. The controller was successfully validated in a 95 L upflow-anaerobic-sludge-blanket (UASB) reactor, treating industrial wine wastewater at OLR ranged between 2.0 and 39.2 g COD/L d for 120 days at mesophilic conditions. Higher performance was achieved contrasted with a conventional strategy carried out in a parallel UASB unit.


2019 ◽  
Vol 80 (8) ◽  
pp. 1505-1511 ◽  
Author(s):  
Nathalie Dyane Miranda Slompo ◽  
Larissa Quartaroli ◽  
Grietje Zeeman ◽  
Gustavo Henrique Ribeiro da Silva ◽  
Luiz Antonio Daniel

Abstract Decentralized sanitary wastewater treatment has become a viable and sustainable alternative, especially for developing countries and small communities. Besides, effluents may present variations in chemical oxygen demand (COD), biochemical oxygen demand (BOD) and total nitrogen values. This study describes the feasibility of using a pilot upflow anaerobic sludge blanket (UASB) reactor to treat wastewater with different organic loads (COD), using black water (BW) and sanitary wastewater, in addition to its potential for preserving nutrients for later recovery and/or reuse. The UASB reactor was operated continuously for 95 weeks, with a hydraulic retention time of 3 days. In Phase 1, the reactor treated simulated BW and achieved 77% CODtotal removal. In Phase 2, treating only sanitary wastewater, the CODtotal removal efficiency was 60%. Phase 3 treated simulated BW again, and CODtotal removal efficiency was somewhat higher than in Phase 1, reaching 81%. In Phase 3, the removal of pathogens was also evaluated: the efficiency was 1.96 log for Escherichia coli and 2.13 log for total coliforms. The UASB reactor was able to withstand large variations in the organic loading rate (0.09–1.49 kg COD m−3 d−1), in continuous operation mode, maintaining a stable organic matter removal.


2021 ◽  
Vol 47 (1) ◽  
pp. 174-180
Author(s):  
Henrique Sousa do Nascimento ◽  
Geísa Vieira Vasconcelos Magalhães ◽  
José Demontier Vieira de Souza-Filho ◽  
Ronaldo Stefanutti ◽  
Ari Clecius Alves de Lima ◽  
...  

This study evaluated the use of two anaerobic bioreactors in the production of biogas from malt bagasse waste. Bioreactor B1 was loaded with a mixture of 600mL of anaerobic sludge, 300g of organic waste, taken from an upflow anaerobic sludge blanket (UASB) reactor, and 300g of malt bagasse residue. Bioreactor B2 was loaded with a mixture of 600g of organic waste and 600mL of anaerobic sludge taken from an UASB reactor. The anaerobic digestion processes lasted for 10 weeks and the produced methane fraction was measured in 5 occasions. Bioreactor B1 presented low methane production (7.2%) but Bioreactor B2 showed a much more signif- icant percentage, reaching up to 48.3%. The experiments were capable of reproducing largescale operational conditions, enabling increased results in biogas capturing and processing, strengthening sustainability and energy efficiency. The experiment also showed the importance of studying different types of organic waste, seeking optimization of anaerobic digestion pro- cesses.


1999 ◽  
Vol 39 (5) ◽  
pp. 177-185 ◽  
Author(s):  
Tarek A. Elmitwalli ◽  
Marcel H. Zandvoort ◽  
Grietje Zeeman ◽  
Harry Bruning ◽  
Gatze Lettinga

The treatment of sewage at a temperature of 13°C was investigated in three reactors (each 3.84 litre) a UASB and two anaerobic hybrid (AH) reactors with small sludge granules with an average diameter of 0.73 mm. The media used in the AH reactors were vertical polyurethane foam sheets. The reactors were operated at a HRT of 8 h. The use of small sludge granules and operating the reactors at low upflow velocity (1.8 m/d) improved suspended COD removal efficiencies for the UASB reactor. Moreover, the use of sheets in the AH reactors significantly increased suspended COD removal efficiencies as compared to the UASB and reached to 87% for pre-settled sewage treatment. The treatment of pre-settled sewage instead of raw sewage in AH reactors significantly increased colloidal and dissolved COD removal efficiencies with 13% and 12% respectively and colloidal COD removal efficiency for the UASB reactor with 13%. At ‘steady state’ for pre-settled sewage treatment, the AH reactors removed 64% of the total COD which is significantly higher by 4% than the UASB reactor. Therefore, the anaerobic treatment of domestic sewage at low temperature can be improved by treating pre-settled sewage in shallow AH reactors containing small sludge granules.


2002 ◽  
Vol 45 (10) ◽  
pp. 213-218 ◽  
Author(s):  
I. Angelidaki ◽  
B.K. Ahring ◽  
H. Deng ◽  
J.E. Schmidt

Combined anaerobic digestion of olive oil mill effluent (OME) with swine manure, was investigated. In batch experiments was shown that for anaerobic degradation of OME alone nitrogen addition was needed. A COD:N ratio in the range of 65:1 to 126:1 was necessary for the optimal degradation process. Furthermore, it was found that methane productions rates during digestion of either swine manure alone or OME alone were much lower than the rates achieved when OME and manure were digested together. Admixing OME with manure at a concentration of 5 to 10% OME resulted in the highest methane production rates. Using upflow anaerobic sludge blanket (UASB) reactors, it was shown that codigestion of OME with swine manure (up to 50% OME) was successful with a COD reduction up to 75%. The process was adapted for degradation of OME with stepwise increase of the OME load to the UASB reactor. The results showed that the high content of ammonia in swine manure, together with content of other nutrients, make it possible to degrade OME without addition of external alkalinity and without addition of external nitrogen source. Anaerobic treatment of OME in UASB reactors resulted in reduction of simple phenolic compounds such as mequinol, phenyl ethyl alcohol and ethyl methyl phenol. After anaerobic treatment the concentration of these compounds was reduced between 75 and 100%. However, the concentration of some degradation products such as methyl phenol and ethyl phenol were detected in significantly higher concentrations after treatment, indicating that the process has to be further optimised to achieve satisfactory removal of all xenobiotic compounds.


1991 ◽  
Vol 24 (3-4) ◽  
pp. 149-160 ◽  
Author(s):  
J. Rintala ◽  
J. L. Sanz Martin ◽  
G. Lettinga

Anaerobic treatment of sulfate - rich (COD/SO4 ratio 1.4-2.1) clarified Whitewater from a thermomechanical pulping (TMP) process was studied in three laboratory-scale upflow anaerobic sludge blanket (UASB) reactors at 55°C and in batch digesters at 55° and 65°C. Different seed materials were used in the UASB reactors. The highest COD removal efficiency (effluent sulfide stripped) achieved was approximately 65 % in the UASB reactors. About 55 % COD removal efficiency was obtained at a loading rate of about 41 kgCODm−3d−1 in the UASB reactor seeded with thermophilic sludge cultivated with volatile fatty acids (VFAs). The total sulfide present in the liquid phase after anaerobic treatment accounted for approximately 65-78 % and 15-61 % of the removed COD in the batch digesters and the UASB reactors, respectively. Sulfate reduction was almost complete in the batch digesters, whereas about 24-64 % of sulfate was reduced in the UASB reactors. Acetate utilization for sulfate reduction was apparent in the batch digesters, whereas that could not be demonstrated in the UASB reactors. Sulfate reduction in the UASB reactors was obviously substrate limited. In conclusion, thermophilic anaerobic treatment is an alternative for the treatment of warm sulfate rich TMP process water.


2017 ◽  
Vol 8 (1) ◽  
pp. 113-122 ◽  
Author(s):  
Martín Alejandro Iribarnegaray ◽  
María Soledad Rodriguez-Alvarez ◽  
Liliana Beatriz Moraña ◽  
Walter Alfredo Tejerina ◽  
Lucas Seghezzo

Abstract In a case study located in suburban sectors of the metropolitan area of the Lerma Valley (Valle de Lerma), in the province of Salta (Argentina), 24 informal decentralized wastewater treatment systems (DWWTS) were evaluated. The analyzed systems had three general configurations: A, septic tank; B, septic tank combined with upflow anaerobic sludge blanket (UASB) reactor; C, septic tank combined with UASB and a final filtration step. Statistically significant differences (p < 0.05) were observed in effluent quality, measured as total coliforms, thermotolerant coliforms, and chemical oxygen demand (COD). Treatment A was the most inefficient, and was statistically different from B and C; there were no significant differences between the latter two. Thermotolerant coliform concentrations were high in all analyzed systems and did not comply with local discharge standards in soakaway pits or in the ground. The lack of a final disinfection step in these systems is thus a weakness that needs to be addressed. The formal inclusion of DWWTS in urban planning could reduce overall investment costs, as long as the best technologies are selected for each case. Incorporation of DWWTS in formal urban planning requires an open debate in which the social perspectives of all relevant users need to be considered.


2014 ◽  
Vol 2014 ◽  
pp. 1-8 ◽  
Author(s):  
Mauro Berni ◽  
Ivo Dorileo ◽  
Grazielle Nathia ◽  
Tânia Forster-Carneiro ◽  
Daniel Lachos ◽  
...  

The issue of residues and industrial effluents represents an unprecedented environmental challenge in terms of recovery, storage, and treatment. This work discusses the perspectives of treating effluents through anaerobic digestion as well as reporting the experience of using an upflow anaerobic sludge blanket (UASB) reactor as biorefinery annex in a pulp and paper industrial plant to be burned in the boilers. The performance of the reactors has shown to be stable under considerable variations in load and showed a significant potential in terms of biogas production. The reactors UASB treated 3600.00 m3of effluent daily from a production of 150.00 tons. The biogas generation was 234.000 kg/year/mill, equivalent in combustible oil. The results of methane gas generated by the anaerobic system UASB (8846.00 kcal/m3) dislocate the equivalent of 650.0 kg of combustible oil (10000.00 kcal/kg) per day (or 234.000 kg/year). The production of 8846.00 Kcal/m3of energy from biogas can make a run at industrial plant for 2 hours. This substitution can save US$ 128.700 annually (or US$ 550.0 of fuel oil/tons). The companies are invested in the use of the biogas in diesel stationary motors cycle that feed the boilers with water in case of storage electricity.


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