The Stimulation Technology Research and Application in the Heavy Oil Carbonate Reservoir of the Fracture and Cavity

Author(s):  
Jianchun Guo ◽  
Jinzhou Zhao ◽  
Lingming Chen ◽  
Yomgming Li ◽  
Ying Fu
Author(s):  
A.V. Osipov ◽  
◽  
A.O. Esaulov ◽  
M.V. Ibragimova ◽  
V.L. Terentiev ◽  
...  

2013 ◽  
Author(s):  
Nabil Al-Bulushi ◽  
Rifaat Al-Mjeni ◽  
Dhiya Said ◽  
Azzan Al-Yaarubi

Author(s):  
R.N. Diyashev ◽  
G.N. Piyakov ◽  
I.M. Iksanov ◽  
R.F. Gainetdinov ◽  
R.L. Rahimov ◽  
...  

2021 ◽  
Author(s):  
Yong Yang ◽  
Xiaodong Li ◽  
Changwei Sun ◽  
Yuanzhi Liu ◽  
Renkai Jiang ◽  
...  

Abstract The problem of water production in carbonate reservoir is always a worldwide problem; meanwhile, in heavy oil reservoir with bottom water, rapid water breakthrough or high water cut is the development feature of this kind of reservoir; the problem of high water production in infill wells in old reservoir area is very common. Each of these three kinds of problems is difficult to be tackled for oilfield developers. When these three kinds of problems occur in a well, the difficulty of water shutoff can be imagined. Excessive water production will not only reduce the oil rate of wells, but also increase the cost of water treatment, and even lead to well shut in. Therefore, how to solve the problem of produced water from infill wells in old area of heavy oil reservoir with bottom water in carbonate rock will be the focus of this paper. This paper elaborates the application of continuous pack-off particles with ICD screen (CPI) technology in infill wells newly put into production in brown field of Liuhua, South China Sea. Liuhua oilfield is a biohermal limestone heavy oil reservoir with strong bottom water. At present, the recovery is only 11%, and the comprehensive water cut is as high as 96%. Excessive water production greatly reduces the hydrocarbon production of the oil well, which makes the production of the oilfield decrease rapidly. In order to delay the decline of oil production, Liuhua oilfield has adopted the mainstream water shutoff technology, including chemical and mechanical water shutoff methods. The application results show that the adaptability of mainstream water shutoff technology in Liuhua oilfield needs to be improved. Although CPI has achieved good water shutoff effect in the development and old wells in block 3 of Liuhua oilfield, there is no application case in the old area of Liuhua oilfield which has been developed for decades, so the application effect is still unclear. At present, the average water cut of new infill wells in the old area reaches 80% when commissioned and rises rapidly to more than 90% one month later. Considering that there is more remaining oil distribution in the old area of Liuhua oilfield and the obvious effect of CPI in block 3, it is decided to apply CPI in infill well X of old area for well completion. CPI is based on the ICD screen radial high-speed fluid containment and pack-off particles in the wellbore annulus to prevent fluid channeling axially, thus achieving well bore water shutoff and oil enhancement. As for the application in fractured reef limestone reservoir, the CPI not only has the function of wellbore water shutoff, but also fills the continuous pack-off particles into the natural fractures in the formation, so as to achieve dual water shutoff in wellbore and fractures, and further enhance the effect of water shutoff and oil enhancement. The target well X is located in the old area of Liuhua oilfield, which is a new infill well in the old area. This target well with three kinds of water problems has great risk of rapid water breakthrough. Since 2010, 7 infill wells have been put into operation in this area, and the water cut after commissioning is 68.5%~92.6%. The average water cut is 85.11% and the average oil rate is 930.92 BPD. After CPI completion in well X, the water cut is only 26% (1/3 of offset wells) and the oil rate is 1300BPD (39.6% higher than that of offset wells). The target well has achieved remarkable effect of reducing water and increasing oil. In addition, in the actual construction process, a total of 47.4m3 particles were pumped into the well, which is equivalent to 2.3 times of the theoretical volume of the annulus between the screen and the borehole wall. Among them, 20m3 continuous pack-off particles entered the annulus, and 27.4m3 continuous pack-off particles entered the natural fractures in the formation. Through the analysis of CPI completed wells in Liuhua oilfield, it is found out that the overfilling quantity is positively correlated to the effect of water shutoff and oil enhancement.


2021 ◽  
Author(s):  
Mustafa Erkin Gozel ◽  
Serkan Uysal ◽  
Cosan Ayan ◽  
Ugur Yuce ◽  
Egemen Ozturk ◽  
...  

Abstract Bati Raman field, with an original oil in place of 1.85 billion barrels, is a naturally fractured carbonate reservoir containing 9-13 °API extra heavy oil with viscosities varying from 300 to 600 cp. Not only a wide range of pilot EOR schemes including gas, thermal and chemical methods, but also novel IOR applications have been tried in the field. CO2 injection was a game changer for this reservoir which has been the main drive mechanism since 1987. Since then, various techniques are applied to further improve the production performance of the field. This study focuses on the design and outcome of the pilot acid fracturing treatments in selected three wells in the tighter and less fractured southeastern part of the reservoir. State of the art planning included full evaluation of well integrity, cement bond and open hole logs, geomechanics studies augmented with rock mechanics laboratory tests. Laboratory tests were also conducted focusing on sludge/emulsion forming tendencies and acid reaction rates. Using these results, expected fracture dimensions were predicted along with production forecasts. In all wells, pre-frac calibration tests were conducted to assess stress conditions and fracturing parameter optimization. The treatments were then executed, improving the procedure between each well for acid fracturing. Injections schemes were operationally efficient and various diversion techniques were used to mitigate the presence of naturally fractured zones. Pre and post-job temperature logs helped to evaluate each treatment. The results from the wells were very positive; total production rate increased about fivefold, observed within one month after the treatments. No considerable change in water or CO2 production in the wells was observed which had been one of the most important objectives during the candidate selection process. One well was suspended, which turned out to be one of the producers of the field after acid fracturing treatment. Each well had a different post-frac production performance because of its geological characteristics and flow dynamics, making the study more valuable for better understanding of the process. The wells are still on critical observation to assess the nature of the created fractures and their longevity in the long run. Even after twelve to fifteen months of production, which is the breaking point period for fracture closure, the overall production level of the wells was double compared to pre-frac rates. One well still has a fracture dominated production while other two changed back into its pre-frac rates. Based on these results, acid fracturing campaign was extended in the area which is currently under evaluation.


2015 ◽  
Author(s):  
Saleh H. Al-Mutairi ◽  
Ahmad D. Al-Aruri ◽  
Saud F. Al-Otaibi ◽  
Abdullah M. Al-Subaie ◽  
Han-Young Park

2018 ◽  
Author(s):  
Sanjeev Malik ◽  
Mohammed Al Balushi ◽  
Salim Al Salmi ◽  
Aamer Al Belushi ◽  
Faris Al Ismali ◽  
...  

Sign in / Sign up

Export Citation Format

Share Document