Rotating Tension Anchor Improves Cement Bond Quality in Steam Well Applications in a Heavy Oil Field Onshore Germany

2017 ◽  
Author(s):  
Arian Ebrahimi ◽  
Clemens Sieveke ◽  
Helge Martin
2019 ◽  
Vol 10 ◽  
pp. 62-67
Author(s):  
S.M. Durkin ◽  
◽  
I.N. Menshikova ◽  
L.M. Rusin ◽  
A.A. Terentiev ◽  
...  
Keyword(s):  

Author(s):  
L.F. Lamas ◽  
V.E. Botechia ◽  
D.J. Schiozer ◽  
M.L. Rocha ◽  
M. Delshad
Keyword(s):  

2014 ◽  
Author(s):  
Mohammed Omar Al-Manhali ◽  
Mohammed Al-rawahi ◽  
Suleiman Mohammed Al-hinai ◽  
Abdullah Alwazeer ◽  
Simon John Brissenden ◽  
...  
Keyword(s):  

2014 ◽  
Vol 644-650 ◽  
pp. 5142-5145 ◽  
Author(s):  
Peng Luo

China is rich in resources of heavy oil.But some oilfield heavy oil reservoir in the development process will encounter interlining, affecting the development effect. In the process of SAGD to carry out the basic research of reservoir interlayer is helpful to identify the basic attributes of reservoir in the interlayer. The interlayer of SAGD development process is helpful to find the study focus and direction of development. Steam chamber breakthrough research achievements of interlining research abroad, summarizes the steam chamber breakthrough interlining, provide technical support for the oil field SAGD breakthrough interlining, it is of great significance for promoting SAGD efficient development.


2021 ◽  
Author(s):  
Siti Najmi Farhan binti Zulkipli

Abstract Addressing wellbore integrity through cement evaluation has been an evergreen topic which frequently catches major operators by surprise due to premature water or gas breakthrough causing low production attainability from the wells. Managing idle well strings arising from integrity issues is also a challenge throughout the production period. The remedial solutions to these issues do not come conveniently and require high cost during late life well intervention which often erodes the well economic limit. A critical element of wellbore barrier which is cement integrity evaluation is proposed to be uplifted and given a new perspective to define success criteria for producer wells to achieve certain reserves addition and production recovery. This paper will highlight integrated factors affecting cement bond quality, impact to well production, potential remedies for poor cement bond observed leveraging on the enhanced workflow and new technology and way forward to proactively prevent the unwanted circumstances in the first opportunity taken. A set of recommendations and prioritization criteria for future cement improvement will be also highlighted. Several case specific wells logged with variable cement bond evaluation tools are re-assessed and deep-dived to trace the root causes for unsatisfactory cement bond quality observed which include reservoir characteristics, understanding anomalies during drilling and cementing operation, identifying cement recipe used, log processing parameters applied and observing best practices during cementing operation to improve the quality. New and emerging cement evaluation technology inclusive of radioactive-based logging to meet specific well objectives will be also briefly discussed in terms of differences and technical deliverables. Looking at each spectrum, results show that there are several interdependent factors contributing to poor cement bond quality observed. Accurate understanding of formation behavior, designing fit-for-purpose cement recipe and adequate planning for cementing operation on well-by-well basis are among the top- notch approaches to be applied for an acceptable cement bond quality and placement. Statistics show that 27% to 64% of production attainability is achieved by wells with good cement quality within the first 3 months of production and this increases to 85% to 98% up until 7 months of production period, while only 12% production attainability achieved for those wells with adverse cement quality issue. In another well, water cut as high as 47% since the first day of production is observed which keeps increasing up to 40% thereafter. In a nutshell, cement evaluation exercise shall not be treated as vacuum, instead it requires an integrated foundation and close collaboration to materialize the desired outcomes. Arresting the issue with the right approach in the first place will be the enabler for optimum well performance and productivity to exceed the recovery target.


2021 ◽  
pp. 1-13
Author(s):  
Wang Xiaoyan ◽  
Zhao Jian ◽  
Yin Qingguo ◽  
Cao Bao ◽  
Zhang Yang ◽  
...  

Summary Achieving effective results using conventional thermal recovery technology is challenging in the deep undisturbed reservoir with extra-heavy oil in the LKQ oil field. Therefore, in this study, a novel approach based on in-situ combustion huff-and-puff technology is proposed. Through physical and numerical simulations of the reservoir, the oil recovery mechanism and key injection and production parameters of early-stage ultraheavy oil were investigated, and a series of key engineering supporting technologies were developed that were confirmed to be feasible via a pilot test. The results revealed that the ultraheavy oil in the LKQ oil field could achieve oxidation combustion under a high ignition temperature of greater than 450°C, where in-situ cracking and upgrading could occur, leading to greatly decreased viscosity of ultraheavy oil and significantly improved mobility. Moreover, it could achieve higher extra-heavy-oil production combined with the energy supplement of flue gas injection. The reasonable cycles of in-situ combustion huff and puff were five cycles, with the first cycle of gas injection of 300 000 m3 and the gas injection volume per cycle increasing in turn. It was predicted that the incremental oil production of a single well would be 500 t in one cycle. In addition, the supporting technologies were developed, such as a coiled-tubing electric ignition system, an integrated temperature and pressure monitoring system in coiled tubing, anticorrosion cementing and completion technology with high-temperature and high-pressure thermal recovery, and anticorrosion injection-production integrated lifting technology. The proposed method was applied to a pilot test in the YS3 well in the LKQ oil field. The high-pressure ignition was achieved in the 2200-m-deep well using the coiled-tubing electric igniter. The maximum temperature tolerance of the integrated monitoring system in coiled tubing reached up to 1200°C, which provided the functions of distributed temperature and multipoint pressure measurement in the entire wellbore. The combination of 13Cr-P110 casing and titanium alloy tubing effectively reduced the high-temperature and high-pressure oxygen corrosion of the wellbore. The successful field test of the comprehensive supporting engineering technologies presents a new approach for effective production in deep extra-heavy-oil reservoirs.


2007 ◽  
Author(s):  
Fernando Pacifico Figueiredo ◽  
Celso Cesar M. Branco ◽  
Fabio Prais ◽  
Marcelo Curzio Salomao ◽  
Cristina Cledia Mezzomo
Keyword(s):  

2021 ◽  
Author(s):  
Ali Reham Al-Jabri ◽  
Rouhollah Farajzadeh ◽  
Abdullah Alkindi ◽  
Rifaat Al-Mjeni ◽  
David Rousseau ◽  
...  

Abstract Heavy oil reservoirs remain challenging for surfactant-based EOR. In particular, selecting fine-tuned and cost effective chemical formulations requires extensive laboratory work and a solid methodology. This paper reports a laboratory feasibility study, aiming at designing a surfactant-polymer pilot for a heavy oil field with an oil viscosity of ~500cP in the South of Sultanate of Oman, where polymer flooding has already been successfully trialed. A major driver was to design a simple chemical EOR method, to minimize the risk of operational issues (e.g. scaling) and ensure smooth logistics on the field. To that end, a dedicated alkaline-free and solvent-free surfactant polymer (SP) formulation has been designed, with its sole three components, polymer, surfactant and co-surfactant, being readily available industrial chemicals. This part of the work has been reported in a previous paper. A comprehensive set of oil recovery coreflood tests has then been carried out with two objectives: validate the intrinsic performances of the SP formulation in terms of residual oil mobilization and establish an optimal injection strategy to maximize oil recovery with minimal surfactant dosage. The 10 coreflood tests performed involved: Bentheimer sandstone, for baseline assessments on large plugs with minimized experimental uncertainties; homogeneous artificial sand and clays granular packs built to have representative mineralogical composition, for tuning of the injection parameters; native reservoir rock plugs, unstacked in order to avoid any bias, to validate the injection strategy in fully representative conditions. All surfactant injections were performed after long polymer injections, to mimic the operational conditions in the field. Under injection of "infinite" slugs of the SP formulation, all tests have led to tertiary recoveries of more than 88% of the remaining oil after waterflood with final oil saturations of less than 5%. When short slugs of SP formulation were injected, tertiary recoveries were larger than 70% ROIP with final oil saturations less than 10%. The final optimized test on a reservoir rock plug, which was selected after an extensive review of the petrophysical and mineralogical properties of the available reservoir cores, led to a tertiary recovery of 90% ROIP with a final oil saturation of 2%, after injection of 0.35 PV of SP formulation at 6 g/L total surfactant concentration, with surfactant losses of 0.14 mg-surfactant/g(rock). Further optimization will allow accelerating oil bank arrival and reducing the large PV of chase polymer needed to mobilize the liberated oil. An additional part of the work consisted in generating the parameters needed for reservoir scale simulation. This required dedicated laboratory assays and history matching simulations of which the results are presented and discussed. These outcomes validate, at lab scale, the feasibility of a surfactant polymer process for the heavy oil field investigated. As there has been no published field test of SP injection in heavy oil, this work may also open the way to a new range of field applications.


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