Future Distillate Fuel Trends in Canada and Some Preliminary Gas Turbine Test Results on Tar Sand Products

2009 ◽  
pp. 115-115-15
Author(s):  
RB Whyte ◽  
RG Grimsey ◽  
CAW Glew
Author(s):  
G. L. Touchton ◽  
M. B. Hilt

A method for the measurement of particulate and sulfur oxides emissions has been developed and tested in the laboratory and the field. The development shows that changes in analysis methods, procedures, and materials are necessary in order to adapt standard USEPA methods to gas turbine conditions. In particular, extreme care must be taken to prevent the formation of pseudo particulate from sulfur dioxide. The field results demonstrate that a G.E. MS7001B emits less than 10 lbm/hr of total particulate if the fuel ash and sulfur content are suitably restricted.


1982 ◽  
Vol 104 (2) ◽  
pp. 143-149 ◽  
Author(s):  
W. F. Z. Lee ◽  
D. C. Blakeslee ◽  
R. V. White

A new metering concept of a self-correcting and self-checking turbine meter is described in which a sensor rotor downstream from the main rotor senses and responds to changes in the exit angle of the fluid leaving the main rotor. The output from the sensor rotor is then electronically combined with the output from the main rotor to produce an adjusted output which automatically and continuously corrects to original meter calibration accuracy. This takes place despite changes in retarding torques, bearing wear and/or upstream conditions occurring in field operations over those which were experienced during calibration. The ratio of the sensor rotor output to the main rotor output at operating conditions is also automatically and continuously compared with that at calibration conditions. This provides an indication of the amount of accuracy deviation from initial calibration that is being corrected by the sensor rotor. This concept is studied theoretically and experimentally. Both the theory and test results (laboratory and field) confirm the concept’s validity and practicability.


Author(s):  
S. Aoki ◽  
Y. Tsukuda ◽  
E. Akita ◽  
M. Terazaki ◽  
L. D. McIaurin ◽  
...  

This paper introduces the engineering approach taken in developing the 501FA gas turbine, which is an uprated version of the existing 501F 150MW class gas turbine. The concepts and procedures which were utilized to uprate this gas turbine are also presented. To achieve better performance, new techniques were incorporated which reflected test results and operating experience. No advanced technologies were introduced. Instead, well experienced techniques are adopted so as not to deteriorate reliability. Improvement of the performance was mainly achieved mainly due to the reduction of cooling air. Tip clearances were also optimized based on shop test and field results.


Author(s):  
D. E. Brandt

The MS7001F heavy–duty gas turbine has been designed utilizing advanced analytical methods and a substantial array of component tests. The integrity of the system required that the prototype unit, with its accessories, be rigorously tested under load. The factory load test was completed on May 18, 1988 after 387 hours and 134 start/stop cycles. The MS7001F prototype gas turbine was instrumented with more than 3000 pieces of instrumentation in order to record all critical temperatures, pressures, flows, strains, displacements, and other pertinent data. The load device was a modified MS7001E compressor, which also supplied the means by which the MS7001F prototype compressor’s pressure ratio was increased to provide for surge margin determination. Inlet throttling of the MS7001F compressor allowed for full firing temperature operation, at reduced load. The results of this factory prototype load test are reported in the paper as are observations made during post test teardown.


Author(s):  
Daniel E. Caguiat

The Naval Surface Warfare Center, Carderock Division (NSWCCD) Gas Turbine Emerging Technologies Code 9334 was tasked by NSWCCD Shipboard Energy Office Code 859 to research and evaluate fouling resistant compressor coatings for Rolls Royce Allison 501-K Series gas turbines. The objective of these tests was to investigate the feasibility of reducing the rate of compressor fouling degradation and associated rate of specific fuel consumption (SFC) increase through the application of anti-fouling coatings. Code 9334 conducted a market investigation and selected coatings that best fit the test objective. The coatings selected were Sermalon for compressor stages 1 and 2 and Sermaflow S4000 for the remaining 12 compressor stages. Both coatings are manufactured by Sermatech International, are intended to substantially decrease blade surface roughness, have inert top layers, and contain an anti-corrosive aluminum-ceramic base coat. Sermalon contains a Polytetrafluoroethylene (PTFE) topcoat, a substance similar to Teflon, for added fouling resistance. Tests were conducted at the Philadelphia Land Based Engineering Site (LBES). Testing was first performed on the existing LBES 501-K17 gas turbine, which had a non-coated compressor. The compressor was then replaced by a coated compressor and the test was repeated. The test plan consisted of injecting a known amount of salt solution into the gas turbine inlet while gathering compressor performance degradation and fuel economy data for 0, 500, 1000, and 1250 KW generator load levels. This method facilitated a direct comparison of compressor degradation trends for the coated and non-coated compressors operating with the same turbine section, thereby reducing the number of variables involved. The collected data for turbine inlet, temperature, compressor efficiency, and fuel consumption were plotted as a percentage of the baseline conditions for each compressor. The results of each plot show a decrease in the rates of compressor degradation and SFC increase for the coated compressor compared to the non-coated compressor. Overall test results show that it is feasible to utilize anti-fouling compressor coatings to reduce the rate of specific fuel consumption increase associated with compressor performance degradation.


Author(s):  
M. W. Horner ◽  
A. Caruvana

Final component and technology verification tests have been completed for application to a 2600°F rotor inlet temperature gas turbine. These tests have proven the capability of combustor, turbine hot section, and IGCC fuel systems and controls to operate in a combined cycle plant burning a coal-derived gas fuel at elevated gas turbine inlet temperatures (2600–3000°F). This paper presents recent test results and summarizes the overall progress made during the DOE-HTTT Phase II program.


1980 ◽  
Author(s):  
T. M. Liu ◽  
R. M. Washam

During the development of a rich-lean staged dry low NOx combustor, the conventional trend of increasing smoke with increasing operating equivalence ratio was found when tests were run with distillate fuel (%H = 13.0). However, when tests were run with residual fuel (%H = 11.4), the trend was reversed. In addition, when the same combustor was run with blends of distillate fuel and residual fuel, a drastic improvement of smoke was observed when only 6 percent of residual fuel was mixed with distillate fuel, and for any blending of more than 10 percent of residual fuel the combustor was practically smoke free. A chemical analysis of fuel samples revealed an appreciable amount of trace metals in the residual fuel, giving rise to the suspicion that the smoke reduction may have been due in part to these trace metals. Of these elements found, vanadium is believed to be the most likely to cause smoke reduction because of its relatively high concentration.


Author(s):  
W. Schmitt ◽  
V. Thomas

The first part of this paper describes the test installation of the gas turbine and the compressor in the workshop, test execution, measuring methods, evaluation and measuring uncertainties. The second part of this paper describes the site installation, execution of the test under full load conditions on natural gas, measuring methods, evaluation and measuring uncertainties. The third part of this paper compares both the measurements and the Reynolds number correction which was used for the evaluation of the pipeline compressor test results in the workshop.


Author(s):  
Klaus Brun ◽  
Rainer Kurz

Field testing of gas turbine compressor packages requires the accurate determination of efficiency, capacity, head, power and fuel flow in sometimes less than ideal working environments. Nonetheless, field test results have significant implication for the compressor and gas turbine manufacturers and their customers. Economic considerations demand that the performance and efficiency of an installation are verified to assure a project’s return on investment. Thus, for the compressor and gas turbine manufacturers, as well as for the end-user, an accurate determination of the field performance is of vital interest. This paper describes an analytic method to predict the measurement uncertainty and, thus, the accuracy, of field test results for gas turbine driven compressors. Namely, a method is presented which can be employed to verify the validity of field test performance results. The equations governing the compressor and gas turbine performance uncertainties are rigorously derived and results are numerically compared to actual field test data. Typical field test measurement uncertainties are presented for different sets of instrumentation. Test parameters that correlate to the most significant influence on the performance uncertainties are identified and suggestions are provided on how to minimize their measurement errors. The effect of different equations of state on the calculated performance is also discussed. Results show that compressor efficiency uncertainties can be unacceptably high when some basic rules for accurate testing are violated. However, by following some simple measurement rules and maintaining commonality of the gas equations of state, the overall compressor package performance measurement uncertainty can be limited and meaningful results can be achieved.


1993 ◽  
Author(s):  
S. Amagasa ◽  
K. Shimomura ◽  
M. Kadowaki ◽  
K. Takeishi ◽  
H. Kawai ◽  
...  

This paper describes the summary of a three year development program for the 1st stage stationary vane and rotating blade for the next generation, 1500°C Class, high efficiency gas turbine. In such a high temperature gas turbine, the 1st turbine vane and blade are the most important hot parts. Full coverage film cooling (FCFC) is adopted for the cooling scheme, and directionally solidified (DS) nickel base super-alloy and thermal barrier coating (TBC) will be used to prolong the creep and thermal fatigue life. The concept of the cooling configuration, fundamental cascade test results and material test results will be presented.


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