Factors controlling prolific gas production from low-permeability sandstone reservoirs: Implications for resource assessment, prospect development, and risk analysis

AAPG Bulletin ◽  
2004 ◽  
Vol 88 (8) ◽  
pp. 1083-1121 ◽  
Author(s):  
Keith W. Shanley ◽  
Robert M. Cluff ◽  
John W. Robinson
SPE Journal ◽  
2007 ◽  
Vol 12 (04) ◽  
pp. 397-407 ◽  
Author(s):  
Mashhad Mousa Fahes ◽  
Abbas Firoozabadi

Summary Wettability of two types of sandstone cores, Berea (permeability on the order of 600 md), and a reservoir rock (permeability on the order of 10 md), is altered from liquid-wetting to intermediate gas-wetting at a high temperature of 140C. Previous work on wettability alteration to intermediate gas-wetting has been limited to 90C. In this work, chemicals previously used at 90C for wettability alteration are found to be ineffective at 140C. New chemicals are used which alter wettability at high temperatures. The results show that:wettability could be permanently altered from liquid-wetting to intermediate gas-wetting at high reservoir temperatures,wettability alteration has a substantial effect on increasing liquid mobility at reservoir conditions,wettability alteration results in improved gas productivity, andwettability alteration does not have a measurable effect on the absolute permeability of the rock for some chemicals. We also find the reservoir rock, unlike Berea, is not strongly water-wet in the gas/water/rock system. Introduction A sharp reduction in gas well deliverability is often observed in many low-permeability gas-condensate reservoirs even at very high reservoir pressure. The decrease in well deliverability is attributed to condensate accumulation (Hinchman and Barree 1985; Afidick et al. 1994) and water blocking (Engineer 1985; Cimolai et al. 1983). As the pressure drops below the dewpoint, liquid accumulates around the wellbore in high saturations, reducing gas relative permeability (Barnum et al. 1995; El-Banbi et al. 2000); the result is a decrease in the gas production rate. Several techniques have been used to increase gas well deliverability after the initial decline. Hydraulic fracturing is used to increase absolute permeability (Haimson and Fairhurst 1969). Solvent injection is implemented in order to remove the accumulated liquid (Al-Anazi et al. 2005). Gas deliverability often increases after the reduction of the condensate saturation around the wellbore. In a successful methanol treatment in Hatter's Pond field in Alabama (Al-Anazi et al. 2005), after the initial decline in well deliverability by a factor of three to five owing to condensate blocking, gas deliverability increased by a factor of two after the removal of water and condensate liquids from the near-wellbore region. The increased rates were, however, sustained for a period of 4 months only. The approach is not a permanent solution to the problem, because the condensate bank will form again. On the other hand, when hydraulic fracturing is used by injecting aqueous fluids, the cleanup of water accumulation from the formation after fracturing is essential to obtain an increased productivity. Water is removed in two phases: immiscible displacement by gas, followed by vaporization by the expanding gas flow (Mahadevan and Sharma 2003). Because of the low permeability and the wettability characteristics, it may take a long time to perform the cleanup; in some cases, as little as 10 to 15% of the water load could be recovered (Mahadevan and Sharma 2003; Penny et al. 1983). Even when the problem of water blocking is not significant, the accumulation of condensate around the fracture face when the pressure falls below dewpoint pressure could result in a reduction in the gas production rate (Economides et al. 1989; Sognesand 1991; Baig et al. 2005).


Energies ◽  
2019 ◽  
Vol 12 (2) ◽  
pp. 327 ◽  
Author(s):  
Qian Wang ◽  
Shenglai Yang ◽  
Haishui Han ◽  
Lu Wang ◽  
Kun Qian ◽  
...  

The petrophysical properties of ultra-low permeability sandstone reservoirs near the injection wells change significantly after CO2 injection for enhanced oil recovery (EOR) and CO2 storage, and different CO2 displacement methods have different effects on these changes. In order to provide the basis for selecting a reasonable displacement method to reduce the damage to these high water cut reservoirs near the injection wells during CO2 injection, CO2-formation water alternate (CO2-WAG) flooding and CO2 flooding experiments were carried out on the fully saturated formation water cores of reservoirs with similar physical properties at in-situ reservoir conditions (78 °, 18 MPa), the similarities and differences of the changes in physical properties of the cores before and after flooding were compared and analyzed. The measurement results of the permeability, porosity, nuclear magnetic resonance (NMR) transversal relaxation time (T2) spectrum and scanning electron microscopy (SEM) of the cores show that the decrease of core permeability after CO2 flooding is smaller than that after CO2-WAG flooding, with almost unchanged porosity in both cores. The proportion of large pores decreases while the proportion of medium pores increases, the proportion of small pores remains almost unchanged, the distribution of pore size of the cores concentrates in the middle. The changes in range and amplitude of the pore size distribution in the core after CO2 flooding are less than those after CO2-WAG flooding. After flooding experiments, clay mineral, clastic fines and salt crystals adhere to some large pores or accumulate at throats, blocking the pores. The changes in core physical properties are the results of mineral dissolution and fines migration, and the differences in these changes under the two displacement methods are caused by the differences in three aspects: the degree of CO2-brine-rock interaction, the radius range of pores where fine migration occurs, the power of fine migration.


2005 ◽  
Vol 127 (3) ◽  
pp. 240-247 ◽  
Author(s):  
D. Brant Bennion ◽  
F. Brent Thomas

Very low in situ permeability gas reservoirs (Kgas<0.1mD) are very common and represent a major portion of the current exploitation market for unconventional gas production. Many of these reservoirs exist regionally in Canada and the United States and also on a worldwide basis. A considerable fraction of these formations appear to exist in a state of noncapillary equilibrium (abnormally low initial water saturation given the pore geometry and capillary pressure characteristics of the rock). These reservoirs have many unique challenges associated with the drilling and completion practices required in order to obtain economic production rates. Formation damage mechanisms affecting these very low permeability gas reservoirs, with a particular emphasis on relative permeability and capillary pressure effects (phase trapping) will be discussed in this article. Examples of reservoirs prone to these types of problems will be reviewed, and techniques which can be used to minimize the impact of formation damage on the productivity of tight gas reservoirs of this type will be presented.


1981 ◽  
Vol 21 (1) ◽  
pp. 137
Author(s):  
B. Wilkinson ◽  
L. Barro

Vast reserves of gas-bearing coal deposits are located in Queensland. Owing to the extremely low permeability and porosity of the coal, very low gas flow rates are normally encountered. In an effort to enhance the gas production to economic quantities and to degasify the coal to provide a safer mining environment, four experimental wells were drilled into coal seams near Blackwater, Queensland.Based on extensive laboratory testing of coal samples, computerised fracture design calculations were performed to determine a suitable stimulation programme. The wells were hydraulically fractured with up to 15 000 US gal of foamed stimulation fluid containing 75 per cent nitrogen. To prop open the induced fracture system, 15 000 lb of sand was pumped with the foam. The maximum concentration was eight pounds of 20-40 mesh sand per gallon of fluid. Gas production from the unstimulated wells was too low to measure. Early production data soon after the fracturing suggested a gas flow rate of approximately 50 Mcf/D.


2019 ◽  
Vol 33 (12) ◽  
pp. 12170-12181 ◽  
Author(s):  
Di Wang ◽  
Shanshan Sun ◽  
Kai Cui ◽  
Hailan Li ◽  
Yejing Gong ◽  
...  

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