scholarly journals Coplanar Waveguide-Fed Broadband Microwave Devices with (or without) a Thin Dielectric Substrate for Use in Flexible Electronic Systems

2014 ◽  
Vol 2014 ◽  
pp. 1-9
Author(s):  
Rafal Lech ◽  
Wojciech Marynowski ◽  
Adam Kusiek ◽  
Jerzy Mazur

Two examples of microwave devices, fed by a coplanar waveguide and realized on a thin substrate (or without such a substrate), are employed to investigate the influence of devices’ curvatures and the proximity of different materials on their parameters. To perform the tests, a broadband antenna and a low-pass filter are chosen. A feeding coplanar waveguide is realized on a dielectric material brick attached to an SMA connector and the main device structure is placed in the air or on a thin substrate. The utilization of a thin substrate or its removal from the structure gives rise to the possibility of placing the devices on curved surfaces. The investigated devices are redesigned and manufactured. The antenna has a total size of 46 mm × 44 mm and covers a frequency range of 2.4–35 GHz which gives a 174% fractional bandwidth. The filter has a total size of 50 mm × 80 mm and its bandwidth has a cutoff frequency of 3.4 GHz. The obtained results are verified by measurements and good agreement is achieved.

2013 ◽  
Vol 562-565 ◽  
pp. 1132-1136
Author(s):  
Xiao Wei Liu ◽  
Jian Yang ◽  
Song Chen ◽  
Liang Liu ◽  
Rui Zhang ◽  
...  

In this paper, we design a high-order switched capacitor filter for rapid change parameter converter. This design uses a structure which consists of three biquads filter sub-units. The design is a 6th-order SC elliptic low-pass filter, and the sample frequency is 250 kHz. By the MATLAB Simulink simulation, the system can meet the design requirements in the time domain. In this paper, the 6th-order switched capacitor elliptic low-pass filter was implemented under 0.5 um CMOS process and simulated in Cadence. The final simulation results show that the pass-band cutoff frequency is 10 kHz, and the maximum pass-band ripple is about 0.106 dB. The stop-band cutoff frequency is 20 kHz, and the minimum stop-band attenuation is 74.78 dB.


1993 ◽  
Vol 6 (12) ◽  
pp. 715-717 ◽  
Author(s):  
Sridhar Kanamaluru ◽  
Ming-Yi Li ◽  
Kai Chang

Author(s):  
Yahya Ahmed Alamri ◽  
Nik Rumzi Nik Idris ◽  
Ibrahim Mohd. Alsofyani ◽  
Tole Sutikno

<p>Stator flux estimation using voltage model is basically the integration of the induced stator back electromotive force (emf) signal. In practical implementation the pure integration is replaced by a low pass filter to avoid the DC drift and saturation problems at the integrator output because of the initial condition error and the inevitable DC components in the back emf signal. However, the low pass filter introduces errors in the estimated stator flux which are significant at frequencies near or lower than the cutoff frequency. Also the DC components in the back emf signal are amplified at the low pass filter output by a factor equals to . Therefore, different integration algorithms have been proposed to improve the stator flux estimation at steady state and transient conditions. In this paper a new algorithm for stator flux estimation is proposed for direct torque control (DTC) of induction motor drives. The proposed algorithm is composed of a second order high pass filter and an integrator which can effectively eliminates the effect of the error initial condition and the DC components. The amplitude and phase errors compensation algorithm is selected such that the steady state frequency response amplitude and phase angle are equivalent to that of the pure integrator and the multiplication and division by stator frequency are avoided. Also the cutoff frequency selection is improved; even small value can filter out the DC components in the back emf signal. The simulation results show the improved performance of the induction motor direct torque control drive with the proposed stator flux estimation algorithm. The simulation results are verified by the experimental results.</p>


Sensors ◽  
2019 ◽  
Vol 19 (23) ◽  
pp. 5173 ◽  
Author(s):  
Jorge Pérez-Bailón ◽  
Belén Calvo ◽  
Nicolás Medrano

This paper presents a fully integrated Gm–C low pass filter (LPF) based on a current steering Gm reduction-tuning technique, specifically designed to operate as the output stage of a SoC lock-in amplifier. To validate this proposal, a first-order and a second-order single-ended topology were integrated into a 1.8 V to 0.18 µm CMOS (Complementary Metal-Oxide-Semiconductor) process, showing experimentally a tuneable cutoff frequency that spanned five orders of magnitude, from tens of mHz to kHz, with a constant current consumption (below 3 µA/pole), compact size (<0.0140 mm2/pole), and a dynamic range better than 70 dB. Compared to state-of-the-art solutions, the proposed approach exhibited very competitive performances while simultaneously fully satisfying the demanding requirements of on-chip portable measurement systems in terms of highly efficient area and power. This is of special relevance, taking into account the current trend towards multichannel instruments to process sensor arrays, as the total area and power consumption will be proportional to the number of channels.


2012 ◽  
Vol 54 (3) ◽  
pp. 732-735 ◽  
Author(s):  
P. Kurgan ◽  
A. Bekasiewicz ◽  
M. Pietras ◽  
M. Kitlinski

2014 ◽  
Vol 609-610 ◽  
pp. 1072-1076
Author(s):  
Qiu Ye Lv ◽  
Chong He ◽  
Wen Jie Fan ◽  
Yu Feng Zhang ◽  
Xiao Wei Liu

In this Paper, a 4th-Order Low-Pass Gm-C Filter is Presented. for the Design of Operational Tranconductance Amplifier(OTA), it Adopts the Techniques of Current Division and Current Cancellation. these Techniques can Help to Achieve a Low Transconductance Value. for the Architecture of the 4th-Order Gm-C Filter, it Consists of Two Biquads. the Two Biquads are Cascade Connected. the Gm-C Low-Pass Filter has been Implemented under 0.5 μm CMOS Process Model. the Final Simulation Results Show the Cutoff Frequency of the Filter is 100Hz and the Stop-Band Attenuation is Larger than 60dB. the Power Consumption is Lower than 1mW and the Total Harmonic Distortion(THD) is -55dB.


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