Computational Study to Identify Feasible Operating Space for a Mixed Mode Combustion Strategy: A Pathway for PCI High Load Operation

Author(s):  
Chaitanya Kavuri ◽  
Sage L. Kokjohn

Mixed mode combustion strategies have shown great potential to achieve high load operation but soot emissions were found to be problematic. A recent study investigating soot emissions in such strategies showed that delaying the load extension injection sufficiently late after the primary heat release makes the soot production dependent solely on the temperature field inside the combustion chamber and eliminates any dependence on mixing time and oxygen availability. The current study focuses on furthering this research to identify a feasible operating space to operate in and enable high load operation with this mixed mode combustion strategy. A PCI combustion event was achieved using a premixed charge of gasoline (early cycle injection) and a load extension injection of gasoline was added near top dead center. CFD modeling considering polycyclic aromatic hydrocarbon (PAH) chemistry up to pyrene was used to perform a full factorial design of experiments (DOE) to study the effects of premixed fuel fraction (fraction of total fuel that is premixed), load extension injection timing and exhaust gas recirculation (EGR). The early injection timings for EGR rates less than 40% showed a soot-NOx tradeoff which constrained operating with SOI timings before TDC. The late injection timings showed reductions in soot and NOx at the expense of gross indicated efficiency (GIE). GIE increased with increasing premixed fuel until the premixed fuel quantity reached 80% of the total fuel mass. Premixed fuel quantities higher than 80% resulted in an efficiency penalty due to increased wall heat transfer losses resulting from early combustion phasing. However, at premixed fuel quantities close to 80%, the peak pressure rise rate became the dominating constraint. This confined the feasible operating space to a premix fuel mass range of 70% to 80%. For this premix fuel mass range, the feasible operating space had two regions; one in the early SOI regime before TDC at EGR rates higher than 38% and the other in the late SOI regime (SOI > 15° ATDC) across the entire EGR space. The study was repeated by splitting the premixed fuel into an early cycle injection and a stratified injection with SOI timing of −70° ATDC. The ratio of fuel in the two injections was varied in the DOE. The results showed that adding a stratified injection increases the ignition delay due to in-cylinder equivalence ratio stratification and relaxes the pressure rise rate effect on the operating space. This allows operation at high premix fuel quantities of 70% and higher with EGR rates less than 40% which yields significant increase in GIE. It was also identified that by targeting the fuel from the stratified injection into the squish region, there is improved oxygen availability in the bowl for the load extension injection, which results in the reduction of soot emissions. This allows the load extension injection to be brought closer to TDC while meeting the soot constraint, which further improves the GIE. Finally, the results from the study were used to demonstrate high load operation at 20 bar and 1300 rpm.

2018 ◽  
Vol 140 (8) ◽  
Author(s):  
Chaitanya Kavuri ◽  
Sage L. Kokjohn

A mixed mode combustion strategy with a premixed compression ignition (PCI) combustion event and a mixing controlled load extension injection was investigated in the current study. Computational fluid dynamics (CFD) modeling was used to perform a full factorial design of experiments (DOE) to study the effects of premixed fuel fraction, load extension injection timing, and exhaust gas recirculation (EGR). The goal of the study was to identify a feasible operating space and demonstrate a pathway to enable high-load operation with the mixed mode combustion strategy. The gross-indicated efficiency (GIE) increased with premix fraction, but the maximum premix fraction was constrained by pressure rise rate which confined the feasible operating space to a premix fuel mass range of 70–80%. Injecting part of the premixed fuel as a stratified injection relieved the pressure rise rate constraint considerably through in-cylinder equivalence ratio stratification. This allowed operation with premix fuel mass of 70% and higher and EGR rates less than 40% which resulted in improved GIE of the late cycle injection cases. It was also identified that by targeting the fuel from the stratified injection into the squish region, there is improved oxygen availability in the bowl for the load extension injection, which resulted in reduced soot emissions. This allowed the load extension injection to be brought closer to top dead center while meeting the soot constraint, which further improved the GIE. Finally, the results from the study were used to demonstrate high-load operation at 20 bar and 1300 rev/min.


2018 ◽  
Vol 144 ◽  
pp. 437-443 ◽  
Author(s):  
Sanghyun Chu ◽  
Jeongwoo Lee ◽  
Jaegu Kang ◽  
Yoonwoo Lee ◽  
Kyoungdoug Min

Author(s):  
Tianhao Yang ◽  
Lianhao Yin ◽  
Gabriel Ingesson ◽  
Per Tunestal ◽  
Rolf Johansson ◽  
...  

Author(s):  
Vittorio Manente ◽  
Bengt Johansson ◽  
Pert Tunestal

Exhaust gas recirculation (EGR) sweeps were performed on ethanol partially premixed combustion (PPC) to show different emission and efficiency trends as compared with diesel PPC. The sweeps showed that when the EGR rate is increased, the efficiency does not diminish, HC trace is flat, and CO is low even with 45% of EGR. NOx exponentially decreases by increasing EGR while soot levels are nearly zero throughout the sweep. The EGR sweeps underlined that at high EGR levels, the pressure rise rate is a concern. To overcome this problem and keep high efficiency and low emissions, a sweep in the timing of the pilot injection and pilot-main ratio was done at ∼16.5 bars gross IMEP. It was found that with a pilot-main ratio of 50:50, and by placing the pilot at −60 with 42% of EGR, NOx and soot are below EURO VI levels; the indicated efficiency is 47% and the maximum pressure rise rate is below 10 bar/CAD. Low load conditions were examined as well. It was found that by placing the start of injection at −35 top dead center, the efficiency is maximized, on the other hand, when the injection is at −25, the emissions are minimized, and the efficiency is only 1.64% lower than its optimum value. The idle test also showed that a certain amount of EGR is needed in order to minimize the pressure rise rate.


Author(s):  
Mohamed Y. E. Selim ◽  
M. S. Radwan ◽  
H. E. Saleh

The use of Jojoba Methyl Ester as a pilot fuel was investigated for almost the first time as a way to improve the performance of dual fuel engine running on natural gas or LPG at part load. The dual fuel engine used was Ricardo E6 variable compression diesel engine and it used either compressed natural gas (CNG) or liquefied petroleum gas (LPG) as the main fuel and Jojoba Methyl Ester as a pilot fuel. Diesel fuel was used as a reference fuel for the dual fuel engine results. During the experimental tests, the following have been measured: engine efficiency in terms of specific fuel consumption, brake power output, combustion noise in terms of maximum pressure rise rate and maximum pressure, exhaust emissions in terms of carbon monoxide and hydrocarbons, knocking limits in terms of maximum torque at onset of knocking, and cyclic data of 100 engine cycle in terms of maximum pressure and its pressure rise rate. The tests examined the following engine parameters: gaseous fuel type, engine speed and load, pilot fuel injection timing, pilot fuel mass and compression ratio. Results showed that using the Jojoba fuel with its improved properties has improved the dual fuel engine performance, reduced the combustion noise, extended knocking limits and reduced the cyclic variability of the combustion.


Author(s):  
Vittorio Manente ◽  
Bengt Johansson ◽  
Pert Tunestal

EGR sweeps were performed on Ethanol Partially Premixed Combustion, PPC, to show different emission and efficiency trends as compared to Diesel PPC. The sweeps showed that increasing the EGR rate the efficiency does not diminish, HC trace is flat and CO is low even with 45% of EGR. NOx exponentially decreases by increasing EGR while soot levels are nearly zero throughout the sweep. The EGR sweeps underlined that at high EGR levels, the pressure rise rate is a concern. To overcome this problem and keep high efficiency and low emissions a sweep in timing of the pilot injection and pilot-main ratio was done at ∼16.5 bar gross IMEP. It was found that with a pilot-main ratio of 50–50 and by placing the pilot at −60 with 42% of EGR, NOx and soot are below EURO VI levels, the indicated efficiency is 47% and the maximum pressure rise rate is below 10 bar/CAD. Low load conditions were examined as well. It was found that by placing the SOI at −35 TDC the efficiency is maximized on the other hand when the injection is at −25 the emissions are minimized and the efficiency is only 1.64% lower than its optimum value. The idle test also showed that a certain amount of EGR is needed in order to minimize the pressure rise rate.


Author(s):  
Dan Wu ◽  
Jian Deng ◽  
Sijia Du ◽  
Libo Qian

Abstract In an over pressure accident, one or more pressurizer safety (or relief) valves will open due to the rapid pressure rise process. Once the safety (or relief) valves are open, the liquid seal will be discharged, and this will generate great discharge force to the downstream pipes. Multi-level protection is chosen using pressurizer safety (or relief) valves with different setpoint in most of Nuclear Power Plant, especially in the self-designed Generation-III Nuclear Power Plants. As the over pressure accident progresses, one or more safety (or relief) valves will be open. The downstream pipes will experience one or more times of impacts, which will influence the arrangement of the pipes. The whole discharge process is very complex, and the key influence factors are the pressure rise rate, safety (or relief) valve opening time, liquid seal temperature and volume, and the arrangement of the downstream discharge pipes. In present paper, liquid seal discharge process in an over pressure accident is studied. The pressure rise rate is so fast that three safety (or relief) valves will open one after another, which will generate three impacts on the downstream discharge pipes. It is found that for a specific design of Nuclear Power Plant, well design of the safety (or relief) valve setpoint is very important to the discharge force analysis results.


2020 ◽  
Vol 257 ◽  
pp. 114018 ◽  
Author(s):  
Jacek Hunicz ◽  
Maciej Mikulski ◽  
Michal S. Geca ◽  
Arkadiusz Rybak

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