Compression Ignition Linear Engine Design Variable Effects

Author(s):  
Csaba To´th-Nagy ◽  
Parviz Farmouri ◽  
Nigel N. Clark

A linear engine/alternator was simulated and designed, and a prototype was built at West Virginia University. This paper describes the engine and presents original operational data. The linear engine was a two-cylinder, two-stroke, common rail direct injection, compression ignition engine. The engine was built using off the shelf components to reduce cost where it was possible. Engine control, injection duration and timing, were achieved using a microcontroller with piston position as a control input. Experiments on the engine were performed to study its behavior. The studied variables included mass of the translator, amount of fuel injected, injection timing, load, and stroke with operating frequency and mechanical efficiency as the basis of comparison. At this point of development, the engine was far from optimized; however, the trends in engine behavior were clear. Increasing the translator mass resulted in decreased operating frequency. Increasing the stroke length also resulted in decreased operating frequency. Overcharging and increased fueling rate, both, resulted in increased power output, efficiency, and operating frequency. Advancing injection timing resulted in increased frequency, efficiency and power output, and decreased stalling frequency. This suggests that the engine operated in an HCCI-like fashion.

Author(s):  
Shouvik Dev ◽  
Tongyang Gao ◽  
Xiao Yu ◽  
Mark Ives ◽  
Ming Zheng

Homogeneous charge compression ignition (HCCI) has been considered as an ideal combustion mode for compression ignition (CI) engines due to its superb thermal efficiency and low emissions of nitrogen oxides (NOx) and particulate matter. However, a challenge that limits practical applications of HCCI is the lack of control over the combustion rate. Fuel stratification and partially premixed combustion (PPC) have considerably improved the control over the heat release profile with modulations of the ratio between premixed fuel and directly injected fuel, as well as injection timing for ignition initiation. It leverages the advantages of both conventional direct injection compression ignition and HCCI. In this study, neat n-butanol is employed to generate the fuel stratification and PPC in a single cylinder CI engine. A fuel such as n-butanol can provide additional benefits of even lower emissions and can potentially lead to a reduced carbon footprint and improved energy security if produced appropriately from biomass sources. Intake port fuel injection (PFI) of neat n-butanol is used for the delivery of the premixed fuel, while the direct injection (DI) of neat n-butanol is applied to generate the fuel stratification. Effects of PFI-DI fuel ratio, DI timing, and intake pressure on the combustion are studied in detail. Different conditions are identified at which clean and efficient combustion can be achieved at a baseline load of 6 bar IMEP. An extended load of 14 bar IMEP is demonstrated using stratified combustion with combustion phasing control.


2020 ◽  
pp. 146808742097355
Author(s):  
Vincent Giuffrida ◽  
Michele Bardi ◽  
Mickael Matrat ◽  
Anthony Robert ◽  
Guillaume Pilla

This paper aims at taking into account the chemistry of O3 in a 3D CFD simulation of compression ignition engine with Diesel type combustion for low load operating points. The methodology developed in this work includes 0D homogeneous reactors simulations, 3D RANS simulations and validation regarding experimental results. The 0D simulations were needed to take into account O3 reactions during the compression stroke because of the high reactivity of O3 with NO and dissociation at high temperature. The values found in these simulations were used as an input in the 3D model to match the correct O3 concentration at fuel injection timing. The 3D simulations were performed using CONVERGETM with a RANS approach. Simulations reproduce the compression/expansion stroke after the intake valve closure to focus on the impact of O3 on the fuel auto ignition. The comparison between numerical and experimental results demonstrates that the proposed methodology is able to capture correctly the impact of O3 addition on ignition delay and on heat release. Moreover, the analysis of the data enables to better understand the fundamental processes driving O3 impact in a CI engine. In particular, using 0D simulations, the plateau effect observed experimentally when increasing O3 concentration is attributed to O3 thermal decomposition and reaction with NO during the compression stroke. Also, 3D CFD results showed that O3 impact is observed mainly during LTHR phase and does not affect the topology and the propagation of the flame inside the combustion chamber.


Energies ◽  
2021 ◽  
Vol 14 (15) ◽  
pp. 4621
Author(s):  
P. A. Harari ◽  
N. R. Banapurmath ◽  
V. S. Yaliwal ◽  
T. M. Yunus Khan ◽  
Irfan Anjum Badruddin ◽  
...  

In the current work, an effort is made to study the influence of injection timing (IT) and injection duration (ID) of manifold injected fuels (MIF) in the reactivity controlled compression ignition (RCCI) engine. Compressed natural gas (CNG) and compressed biogas (CBG) are used as the MIF along with diesel and blends of Thevetia Peruviana methyl ester (TPME) are used as the direct injected fuels (DIF). The ITs of the MIF that were studied includes 45°ATDC, 50°ATDC, and 55°ATDC. Also, present study includes impact of various IDs of the MIF such as 3, 6, and 9 ms on RCCI mode of combustion. The complete experimental work is conducted at 75% of rated power. The results show that among the different ITs studied, the D+CNG mixture exhibits higher brake thermal efficiency (BTE), about 29.32% is observed at 50° ATDC IT, which is about 1.77, 3.58, 5.56, 7.51, and 8.54% higher than D+CBG, B20+CNG, B20+CBG, B100+CNG, and B100+CBG fuel combinations. The highest BTE, about 30.25%, is found for the D+CNG fuel combination at 6 ms ID, which is about 1.69, 3.48, 5.32%, 7.24, and 9.16% higher as compared with the D+CBG, B20+CNG, B20+CBG, B100+CNG, and B100+CBG fuel combinations. At all ITs and IDs, higher emissions of nitric oxide (NOx) along with lower emissions of smoke, carbon monoxide (CO), and hydrocarbon (HC) are found for D+CNG mixture as related to other fuel mixtures. At all ITs and IDs, D+CNG gives higher In-cylinder pressure (ICP) and heat release rate (HRR) as compared with other fuel combinations.


2021 ◽  
pp. 146808742110183
Author(s):  
Jonathan Martin ◽  
André Boehman

Compression-ignition (CI) engines can produce higher thermal efficiency (TE) and thus lower carbon dioxide (CO2) emissions than spark-ignition (SI) engines. Unfortunately, the overall fuel economy of CI engine vehicles is limited by their emissions of nitrogen oxides (NOx) and soot, which must be mitigated with costly, resource- and energy-intensive aftertreatment. NOx and soot could also be mitigated by adding premixed gasoline to complement the conventional, non-premixed direct injection (DI) of diesel fuel in CI engines. Several such “dual-fuel” combustion modes have been introduced in recent years, but these modes are usually studied individually at discrete conditions. This paper introduces a mapping system for dual-fuel CI modes that links together several previously studied modes across a continuous two-dimensional diagram. This system includes the conventional diesel combustion (CDC) and conventional dual-fuel (CDF) modes; the well-explored advanced combustion modes of HCCI, RCCI, PCCI, and PPCI; and a previously discovered but relatively unexplored combustion mode that is herein titled “Piston-split Dual-Fuel Combustion” or PDFC. Tests show that dual-fuel CI engines can simultaneously increase TE and lower NOx and/or soot emissions at high loads through the use of Partial HCCI (PHCCI). At low loads, PHCCI is not possible, but either PDFC or RCCI can be used to further improve NOx and/or soot emissions, albeit at slightly lower TE. These results lead to a “partial dual-fuel” multi-mode strategy of PHCCI at high loads and CDC at low loads, linked together by PDFC. Drive cycle simulations show that this strategy, when tuned to balance NOx and soot reductions, can reduce engine-out CO2 emissions by about 1% while reducing NOx and soot by about 20% each with respect to CDC. This increases emissions of unburnt hydrocarbons (UHC), still in a treatable range (2.0 g/kWh) but five times as high as CDC, requiring changes in aftertreatment strategy.


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