scholarly journals Detailed Examination of a Modified Two-Stage Micro Gas Turbine Combustor

2017 ◽  
Vol 140 (2) ◽  
Author(s):  
Andreas Schwärzle ◽  
Thomas O. Monz ◽  
Andreas Huber ◽  
Manfred Aigner

Jet-stabilized combustion is a promising technology for fuel flexible, reliable, highly efficient combustion systems. The aim of this work is a reduction of NOx emissions of a previously published two-stage micro gas turbine (MGT) combustor (Zanger et al., 2015, “Experimental Investigation of the Combustion Characteristics of a Double-Staged FLOX-Based Combustor on an Atmospheric and a Micro Gas Turbine Test Rig,” ASME Paper No. GT2015-42313 and Schwärzle et al., 2016, “Detailed Examination of Two-Stage Micro Gas Turbine Combustor,” ASME Paper No. GT2016-57730), where the pilot stage (PS) of the combustor was identified as the main contributor to NOx emissions. The geometry optimization was carried out regarding the shape of the pilot dome and the interface between PS and main stage (MS) in order to prevent the formation of high-temperature recirculation zones. Both stages have been run separately to allow a detailed understanding of the flame stabilization within the combustor, its range of stable combustion, the interaction between both stages, and the influence of the modified geometry. All experiments were conducted at atmospheric pressure and an air preheat temperature of 650  °C. The flame was analyzed in terms of shape, length, and lift-off height, using OH* chemiluminescence (OH-CL) images. Emission measurements for NOx, CO, and unburned hydrocarbons (UHC) emissions were carried out. At a global air number of λ = 2, a fuel split variation was carried out from 0 (only PS) to 1 (only MS). The modification of the geometry leads to a decrease in NOx and CO emissions throughout the fuel split variation in comparison with the previous design. Regarding CO emissions, the PS operations are beneficial for a fuel split above 0.8. The local maximum in NOx emissions observed for the previous combustor design at a fuel split of 0.78 was not apparent for the modified design. NOx emissions were increasing, when the local air number of the PS was below the global air number. In order to evaluate the influence of the modified design on the flow field and identify the origin of the emission reduction compared to the previous design, unsteady Reynolds-averaged Navier–Stokes simulations were carried out for both geometries at fuel splits of 0.93 and 0.78, respectively, using the DLR (German Aerospace Center) in-house code turbulent heat release extension of the tau code (theta) with the k–ω shear stress transport turbulence model and the DRM22 (Kazakov and Frenklach, 1995, “DRM22,” University of California at Berkeley, Berkeley, CA, accessed Sept. 21, 2017, http://www.me.berkeley.edu/drm/) detailed reaction mechanism. The numerical results showed a strong influence of the recirculation zones on the PS reaction zone.

Author(s):  
A. Schwärzle ◽  
T. O. Monz ◽  
A. Huber ◽  
M. Aigner

Jet-stabilized combustion is a promising technology for fuel flexible, reliable, highly efficient combustion systems. The aim of this work is a reduction of NOx emissions of a previously published two-staged MGT combustor [1, 2], where the pilot stage of the combustor was identified as the main contributor to NOx emissions. The geometry optimization was carried out regarding the shape of the pilot dome and the interface between pilot and main stage in order to prevent the formation of high temperature recirculation zones. Both stages have been run separately to allow a detailed understanding of the flame stabilization within the combustor, its range of stable combustion, the interaction between both stages and the influence of the modified geometry. All experiments were conducted at atmospheric pressure and an air preheat temperature of 650 °C. The flame was analyzed in terms of shape, length and lift-off height, using OH* chemiluminescence images. Emission measurements for NOx, CO and UHC emissions were carried out. At a global air number of λ = 2, a fuel split variation was carried out from 0 (only pilot-stage) to 1 (only main stage). The modification of the geometry lead to a decrease in NOx and CO emissions throughout the fuel split variation in comparison with the previous design. Regarding CO emissions, the pilot stage operations is beneficial for a fuel split above 0.8. The local maximum in NOx emissions observed for the previous combustor design at a fuel split of 0.78 was not apparent for the modified design. NOx emissions were increasing, when the local air number of the pilot stage was below the global air number. In order to evaluate the influence of the modified design on the flow field and identify the origin of the emission reduction compared to the previous design, unsteady RANS simulations were carried out for both geometries at fuel splits of 0.93 and 0.78, respectively, using the DLR in-house code THETA with the k-w SST turbulence model and the DRM22 [3] detailed reaction mechanism. The numerical results showed a strong influence of the recirculation zones on the pilot stage reaction zone.


Author(s):  
Masato Hiramatsu ◽  
Yoshifumi Nakashima ◽  
Sadamasa Adachi ◽  
Yudai Yamasaki ◽  
Shigehiko Kaneko

One approach to achieving 99% combustion efficiency (C.E.) and 10 ppmV or lower NOx (at 15%O2) in a micro gas turbine (MGT) combustor fueled by biomass gas at a variety of operating conditions is with the use of flameless combustion (FLC). This paper compares experimentally obtained results and CHEMKIN analysis conducted for the developed combustor. As a result, increase the number of stage of FLC combustion enlarges the MGT operation range with low-NOx emissions and high-C.E. The composition of fuel has a small effect on the characteristics of ignition in FLC. In addition, NOx in the engine exhaust is reduced by higher levels of CO2 in the fuel.


Author(s):  
A. Schwärzle ◽  
T. O. Monz ◽  
M. Aigner

Jet-stabilized combustion is a promising technology for fuel flexible, reliable, highly efficient combustion systems. In this work, experiments have been carried out on a two-staged combustor, with a jet-stabilized main stage and a swirl-stabilized pilot stage. Both stages have been run separately to allow a more detailed understanding of the flame stabilization within the combustor and its range of stable operation. All experiments were conducted at atmospheric pressure and preheating temperatures of 650 °C. The air was fed to both stages of the combustor for all experiments. The flame was analyzed in terms of shape, length and lift-off height, using the OH* chemiluminescence signal detected by an ICCD-camera. Emission measurements for NOx, CO and UHC emissions were carried out. The pilot stage was examined at a local air number between 0.14 and 1.43, which corresponds to a global air number of 2.0 to 20.7. For lowest air numbers, the combustor works with the RQL principle with lowest emissions in pilot stage only operation. This is because the remaining fuel fed to the pilot stage mixes rapidly with the air from the main stage and reacts under lean conditions. The optimum operating range of the main stage is at global air numbers between 3 and 3.2 with a blow-off limit beyond λg = 4.0. At a global air number of λg = 2, a fuel split variation was carried out from 0 (only pilot stage) to 1 (only main stage). In combined operation and at higher fuel splits, the NOx emissions are reduced compared to the main stage only operation, while the opposing effect on NOx emissions was observed for lower fuel splits. CFD simulations of the combustor test rig showed higher residence times in the pilot stage compared to the main stage which facilitates higher NOx formation rates in the pilot stage. This could be improved by a geometry optimization. The operation of the pilot stage was beneficial at fuel splits above 90 %, especially concerning an extended operating range to higher global air numbers. In addition, the capability of the combustor to operate at higher thermal power inputs was investigated. Originally designed for the Turbec T100 micro gas turbine, the combustor was operated at 160% of the original design point. At a constant air number, this led to a decrease in NOx and to an increase in CO emissions, caused by shorter residence times in the combustion chamber at higher power input. An operation strategy of constant pilot air number increases the envelope of a stable operation regime further.


2008 ◽  
Vol 3 (1) ◽  
pp. 204-215
Author(s):  
Kousaku YOTORIYAMA ◽  
Shunsuke AMANO ◽  
Hidetomo FUJIWARA ◽  
Tomohiko FURUHATA ◽  
Masataka ARAI

Author(s):  
Chi-Rong Liu ◽  
Hsin-Yi Shih

The purpose of this study is to investigate the combustion and emission characteristics of syngas fuels applied in a micro gas turbine, which is originally designed for a natural gas fired engine. The computation results were conducted by a numerical model, which consists of the three-dimension compressible k–ε model for turbulent flow and PPDF (presumed probability density function) model for combustion process. As the syngas is substituted for methane, the fuel flow rate and the total heat input to the combustor from the methane/syngas blended fuels are varied with syngas compositions and syngas substitution percentages. The computed results presented the syngas substitution effects on the combustion and emission characteristics at different syngas percentages (up to 90%) for three typical syngas compositions and the conditions where syngas applied at fixed fuel flow rate and at fixed heat input were examined. Results showed the flame structures varied with different syngas substitution percentages. The high temperature regions were dense and concentrated on the core of the primary zone for H2-rich syngas, and then shifted to the sides of the combustor when syngas percentages were high. The NOx emissions decreased with increasing syngas percentages, but NOx emissions are higher at higher hydrogen content at the same syngas percentage. The CO2 emissions decreased for 10% syngas substitution, but then increased as syngas percentage increased. Only using H2-rich syngas could produce less carbon dioxide. The detailed flame structures, temperature distributions, and gas emissions of the combustor were presented and compared. The exit temperature distributions and pattern factor (PF) were also discussed. Before syngas fuels are utilized as an alternative fuel for the micro gas turbine, further experimental testing is needed as the modeling results provide a guidance for the improved designs of the combustor.


Author(s):  
Oanh Nguyen ◽  
Scott Samuelsen

In view of increasingly stringent NOx emissions regulations on stationary gas turbines, lean combustion offers an attractive option to reduce reaction temperatures and thereby decrease NOx production. Under lean operation, however, the reaction is vulnerable to blowout. It is herein postulated that pilot hydrogen dopant injection, discretely located, can enhance the lean blowout performance without sacrificing overall performance. The present study addresses this hypothesis in a research combustor assembly, operated at atmospheric pressure, and fired on natural gas using rapid mixing injection, typical of commercial units. Five hydrogen injector scenarios are investigated. The results show that (1) pilot hydrogen dopant injection, discretely located, leads to improved lean blowout performance and (2) the location of discrete injection has a significant impact on the effectiveness of the doping strategy.


2021 ◽  
Vol 0 (0) ◽  
Author(s):  
Vedant Dwivedi ◽  
Srikanth Hari ◽  
S. M. Kumaran ◽  
B. V. S. S. S. Prasad ◽  
Vasudevan Raghavan

Abstract Experimental and numerical study of flame and emission characteristics in a tubular micro gas turbine combustor is reported. Micro gas turbines are used for distributed power (DP) generation using alternative fuels in rural areas. The combustion and emission characteristics from the combustor have to be studied for proper design using different fuel types. In this study methane, representing fossil natural gas, and biogas, a renewable fuel that is a mixture of methane and carbon-dioxide, are used. Primary air flow (with swirl component) and secondary aeration have been varied. Experiments have been conducted to measure the exit temperatures. Turbulent reactive flow model is used to simulate the methane and biogas flames. Numerical results are validated against the experimental data. Parametric studies to reveal the effects of primary flow, secondary flow and swirl have been conducted and results are systematically presented. An analysis of nitric-oxides emission for different fuels and operating conditions has been presented subsequently.


Author(s):  
K. O. Smith ◽  
A. Fahme

Three subscale, cylindrical combustors were rig tested on natural gas at typical industrial gas turbine operating conditions. The intent of the testing was to determine the effect of combustor liner cooling on NOx and CO emissions. In order of decreasing liner cooling, a metal louvre-cooled combustor, a metal effusion-cooled combustor, and a backside-cooled ceramic (CFCC) combustor were evaluated. The three combustors were tested using the same lean-premixed fuel injector. Testing showed that reduced liner cooling produced lower CO emissions as reaction quenching near the liner wall was reduced. A reduction in CO emissions allows a reoptimization of the combustor air flow distribution to yield lower NOx emissions.


Author(s):  
Haoyang Liu ◽  
Wenkai Qian ◽  
Min Zhu ◽  
Suhui Li

Abstract To avoid flashback issues of the high-H2 syngas fuel, current syngas turbines usually use non-premixed combustors, which have high NOx emissions. A promising solution to this dilemma is RQL (rich-burn, quick-mix, lean-burn) combustion, which not only reduces NOx emissions, but also mitigates flashback. This paper presents a kinetics modeling study on NOx emissions of a syngas-fueled gas turbine combustor using RQL architecture. The combustor was simulated with a chemical reactor network model in CHEMKIN-PRO software. The combustion and NOx formation reactions were modeled using a detailed kinetics mechanism that was developed for syngas. Impacts of combustor design/operating parameters on NOx emissions were systematically investigated, including combustor outlet temperature, rich/lean air flow split and residence time split. The mixing effects in both the rich-burn zone and the quick-mix zone were also investigated. Results show that for an RQL combustor, the NOx emissions initially decrease and then increase with combustor outlet temperature. The leading parameters for NOx control are temperature-dependent. At typical modern gas turbine combustor operating temperatures (e.g., < 1890 K), the air flow split is the most effective parameter for NOx control, followed by the mixing at the rich-burn zone. However, as the combustor outlet temperature increases, the impacts of air flow split and mixing in the rich-burn zone on NOx reduction become less pronounced, whereas both the residence time split and the mixing in the quick-mix zone become important.


Sign in / Sign up

Export Citation Format

Share Document