Aerodynamics of a Low-Pressure Turbine Airfoil at Low Reynolds Numbers—Part I: Steady Flow Measurements

2012 ◽  
Vol 135 (1) ◽  
Author(s):  
Ali Mahallati ◽  
Brian R. McAuliffe ◽  
Steen A. Sjolander ◽  
Thomas J. Praisner

This two-part paper presents a detailed experimental investigation of the laminar separation and transition phenomena on the suction surface of a high-lift low-pressure turbine airfoil, PakB. The first part describes the influence of Reynolds number, freestream turbulence intensity and turbulence length scale on the PakB airfoil under steady inflow conditions. The present measurements are distinctive in that a closely-spaced array of hot-film sensors has allowed a very detailed examination of the suction surface boundary layer behavior. In addition, this paper presents a technique for interpreting the transition process in steady, and periodically unsteady, separated flows based on dynamic and statistical properties of the hot-film measurements. Measurements were made in a low-speed linear cascade facility at Reynolds numbers between 25,000 and 150,000 at three freestream turbulence intensity levels of 0.4%, 2%, and 4%. Two separate grids were used to generate turbulence intensity of 4% with integral length scales of about 10% and 40% of the airfoil axial chord length. While the higher levels of turbulence intensity promoted earlier transition and a shorter separation bubble, turbulence length scale did not have a noticeable effect on the transition process. The size of the suction side separation bubble increased with decreasing Reynolds number, and under low freestream turbulence levels the bubble failed to reattach at low Reynolds numbers. As expected, the losses increased with the length of the separation bubble, and increased significantly when the bubble failed to reattach.

Author(s):  
Ali Mahallati ◽  
Brian R. McAuliffe ◽  
Steen A. Sjolander ◽  
Thomas J. Praisner

This two-part paper presents a detailed experimental investigation of the laminar separation and transition phenomena on the suction surface of a high-lift low-pressure (LP) turbine airfoil, PakB. The first part describes the influence of Reynolds number, freestream turbulence intensity and turbulence length scale on the PakB airfoil under steady inflow conditions. The present measurements are distinctive in that a closely-spaced array of hot-film sensors has allowed a very detailed examination to be made of both the steady and unsteady behaviour of the suction surface boundary layer. In addition, this paper presents a technique for interpreting the transition process in steady, and periodically unsteady, separated flows based on dynamic and statistical properties of the hot-film measurements. Measurements were made at Reynolds number varying from 25,000 to 150,000 and for freestream turbulence intensities of 0.4%, 2% and 4%. Two separate grids were used to generate turbulence intensity of 4% with integral length scales of about 10% and 40% of the airfoil axial chord length. The first is comparable with the turbulence length scales expected in the engine and the second is considerably larger. While the higher levels of freestream turbulence intensity promoted earlier transition and a shorter separation bubble, the varying turbulence length scale did not have a noticeable effect on the transition process. The size of the separation bubble increased with decreasing Reynolds number, and under low freestream turbulence levels the bubble failed to reattach at low Reynolds numbers. As expected, the losses increased with the length of the separation bubble on the suction side of the airfoil, and increased significantly when the bubble failed to reattach.


1999 ◽  
Vol 122 (2) ◽  
pp. 431-433 ◽  
Author(s):  
C. G. Murawski ◽  
K. Vafai

An experimental study was conducted in a two-dimensional linear cascade, focusing on the suction surface of a low pressure turbine blade. Flow Reynolds numbers, based on exit velocity and suction length, have been varied from 50,000 to 300,000. The freestream turbulence intensity was varied from 1.1 to 8.1 percent. Separation was observed at all test Reynolds numbers. Increasing the flow Reynolds number, without changing freestream turbulence, resulted in a rearward movement of the onset of separation and shrinkage of the separation zone. Increasing the freestream turbulence intensity, without changing Reynolds number, resulted in shrinkage of the separation region on the suction surface. The influences on the blade’s wake from altering freestream turbulence and Reynolds number are also documented. It is shown that width of the wake and velocity defect rise with a decrease in either turbulence level or chord Reynolds number. [S0098-2202(00)00202-9]


Author(s):  
Christopher G. Murawski ◽  
Rolf Sondergaard ◽  
Richard B. Rivir ◽  
Kambiz Vafai ◽  
Terrence W. Simon ◽  
...  

Low pressure turbines in aircraft experience large changes in flow Reynolds number as the gas turbine engine operates from takeoff to high altitude cruise. Low pressure turbine blades are also subject to regions of strong acceleration and diffusion. These changes in Reynolds number, strong acceleration, as well as elevated levels of turbulence can result in unsteady separation and transition zones on the surface of the blade. An experimental study was conducted in a two-dimensional linear cascade, focusing on the suction surface of a low pressure turbine blade. The intent was to assess the effects of changes in Reynolds number, and freestream turbulence intensity. Flow Reynolds numbers, based on exit velocity and suction surface length, have been varied from 50,000 to 300,000. The freestream turbulence intensity was varied from 1.1 to 8.1 percent. Separation was observed at all test Reynolds numbers. Increasing the flow Reynolds number, without changing freestream turbulence, resulted in a slightly rearward movement of the onset of separation and shrinkage of the separation zone. Increasing the freestream turbulence intensity, without changing Reynolds number resulted in a shrinkage of the separation region on the suction surface. Increasing both flow Reynolds numbers and freestream turbulence intensity compounded these effects such that at a Reynolds number of 300,000 and a freestream turbulence intensity of 8.1%, the separation zone was almost nonexistent. The influences on the blade’s wake from altering freestream turbulence and Reynolds number are also documented. The width of the wake and velocity defect rise with a decrease in either turbulence level or chord Reynolds number. Numerical simulations were performed in support of experimental results. The numerical results compare well qualitatively with the low freestream turbulence experimental cases.


Author(s):  
Kenneth Van Treuren ◽  
Tyler Pharris ◽  
Olivia Hirst

The low-pressure turbine has become more important in the last few decades because of the increased emphasis on higher overall pressure and bypass ratios. The desire is to increase blade loading to reduce blade counts and stages in the low-pressure turbine of a gas turbine engine. Increased turbine inlet temperatures for newer cycles results in higher temperatures in the low-pressure turbine, especially the latter stages, where cooling technologies are not used. These higher temperatures lead to higher work from the turbine and this, combined with the high loadings, can lead to flow separation. Separation is more likely in engines operating at high altitudes and reduced throttle setting. At the high Reynolds numbers found at takeoff, the flow over a low-pressure turbine blade tends to stay attached. At lower blade Reynolds numbers (25,000 to 200,000), found during cruise at high altitudes, the flow on the suction surface of the low-pressure turbine blades is inclined to separate. This paper is a study on the flow characteristics of the L1A turbine blade at three low Reynolds numbers (60,000, 108,000, and 165,000) and 15 turbulence intensities (1.89% to 19.87%) in a steady flow cascade wind tunnel. With this data, it is possible to examine the impact of Reynolds number and turbulence intensity on the location of the initiation of flow separation, the flow separation zone, and the reattachment location. Quantifying the change in separated flow as a result of varying Reynolds numbers and turbulence intensities will help to characterize the low momentum flow environments in which the low-pressure turbine must operate and how this might impact the operation of the engine. Based on the data presented, it is possible to predict the location and size of the separation as a function of both the Reynolds number and upstream freestream turbulence intensity (FSTI). Being able to predict this flow behavior can lead to more effective blade designs using either passive or active flow control to reduce or eliminate flow separation.


Author(s):  
J. W. Douglas ◽  
S.-M. Li ◽  
B. Song ◽  
W. F. Ng ◽  
Toyotaka Sonoda ◽  
...  

Very little published literature documents the effects of different freestream turbulence intensities on compressor flows at realistically high Reynolds numbers. This paper presents a study of these effects on a transonic, linear, compressor stator cascade. The cascade consisted of high turning stator airfoils that had the camber of 55 degrees. The effects of freestream turbulence intensities of approximately 0.1% (baseline) and 1.6% were examined. Inlet Mach numbers to the cascade were tested from 0.55 to 0.89. Reynolds numbers, based on the inlet conditions and blade chord, varied between 1.0–2.0×106. Inlet flow angles to the cascade ranged from a choking to a stall condition. For the baseline cases, at most positive incidence angles to the cascade, surface oil flow visualization and Schlieren pictures showed a significant flow separation on the suction surface of the blade. Under these conditions, the increase in freestream turbulence from 0.1% to 1.6% significantly reduced the flow losses of the cascade (by as much as 57% in some cases). In other test conditions where no evidence depicted flow separation on the blade, there were no measurable effects on the losses due to the increase in freestream turbulence intensity. In addition, the increase of freestream turbulence intensity also improved the effective operating range of the cascade significantly (e.g., by 46% or higher).


Author(s):  
Mounir B. Ibrahim ◽  
Samuel Vinci ◽  
Olga Kartuzova ◽  
Ralph J. Volino

A study of a very high lift, low-pressure turbine airfoil in the presence of unsteady wakes was performed computationally and compared against experimental results. The experiments were conducted in a low speed wind tunnel under high (4.9%) and then low (0.6%) freestream turbulence intensity conditions with a flow coefficient (ζ) of 0.7. The experiments were done on a linear cascade with wakes that were produced from moving rods upstream of the cascade with the rod to blade spacing varied from 1 to 1.6 to 2. In the present study two different Reynolds numbers (25,000 and 50,000, based on the suction surface length and the nominal exit velocity from the cascade) were considered. The experimental and computational data have shown that in cases without wakes, the boundary layer separated and did not reattach. The CFD was performed with Large Eddy Simulation (LES) and Unsteady Reynolds-Averaged Navier-Stokes (URANS), Transition-SST, utilizing the finite-volume code ANSYS FLUENT under the same freestream turbulence and Reynolds number conditions as the experiment but only at a rod to blade spacing of 1. With wakes, separation was largely suppressed, particularly if the wake passing frequency was sufficiently high. Similar effect was predicted by 3D CFD simulations. Computational results for the pressure coefficients and velocity profiles were in a reasonable agreement with experimental ones for all cases examined. The 2D CFD efforts failed to capture the three dimensionality effects of the wake and thus were less consistent with the experimental data. As a further computational study, cases were run to simulate higher wake passing frequencies which were not run experimentally. The results of these computational cases showed that an initial 25% increase from the experimental dimensionless wake passing frequency of F = 0.45 greatly reduced the size of the separation bubble, nearly completely suppressing it, however an additional 33% increase on top of this did not prove to have much of an effect.


Author(s):  
Stephen A. Pym ◽  
Asad Asghar ◽  
William D. E. Allan ◽  
John P. Clark

Abstract Aircraft are operating at increasingly high-altitudes, where decreased air density and engine power settings have led to increasingly low Reynolds numbers in the low-pressure turbine portion of modern-day aeroengines. These operating conditions, in parallel with highly-loaded blade profiles, result in non-reattaching laminar boundary layer separation along the blade suction surface, increasing loss and decreasing engine performance. This work presents an experimental investigation into the potential for integrated leading-edge tubercles to improve blade performance in this operating regime. A turn-table cascade test-section was constructed and commissioned to test a purpose-designed, forward-loaded, low-pressure turbine blade profile at various incidences and Reynolds numbers. Baseline and tubercled blades were tested at axial chord Reynolds numbers at and between 15 000 and 60 000, and angles of incidence ranging from −5° to +10°. Experimental data collection included blade surface pressure measurements, total pressure loss in the blade wakes, hot-wire anemometry, surface hot-film measurements, and surface flow visualization using tufts. Test results showed that the implementation of tubercles did not lead to a performance enhancement. However, useful conclusions were drawn regarding the ability of tubercles to generate stream-wise vortices at ultra-low Reynolds numbers. Additional observations helped to characterize the suction surface boundary layer over the highly-loaded, low-pressure turbine blade profile when at off-design conditions. Recommendations were made for future work.


Author(s):  
Pasquale Cardamone ◽  
Peter Stadtmu¨ller ◽  
Leonhard Fottner

The effects of wake passing on the development of the profile boundary layer of a highly loaded low-pressure turbine cascade are studied using the RANS code TRACE-U. The numerical results are compared with available experimental data to verify the accuracy of the code in predicting the periodic-unsteady transition and separation mechanisms at low Reynolds number conditions. The experimental investigations have been carried out on a turbine cascade called T106D-EIZ subjected to wakes generated by an up-stream moving bar-type generator. The cascade pitch was increased by about 30% with respect to design conditions without modifying the blade geometry in order to obtain a large separation bubble on the suction surface. The extensive database containing time-averaged as well as time-resolved results was presented in a separate paper by Stadtmu¨ller and Fottner (2001) and is discussed only briefly. The time-accurate multistage Navier-Stokes solver TRACE-U developed by the DLR Cologne used for the numerical simulations employs a modified version of the one-equation Spalart-Allmaras turbulence model coupled with a transition correlation based on the work of Abu-Ghannam and Shaw in the formulation of Drela. The objective of this paper is to provide further insight into the aerodynamics of the wake-induced transition process and to rate the application limits of the numerical approach for exit Reynolds numbers as low as 60.000. The CFD predictions for two different flow conditions are compared with the measurements. Plots of wall-shear stress, blade loading, shape factor and loss behaviour are used to verify the reliability of the code. The periodic-unsteady development of the boundary layer as well as the loss behaviour is well reproduced for higher Reynolds numbers. For the case with massive separation, large discrepancies between numerical and experimental results are observed.


2001 ◽  
Vol 124 (1) ◽  
pp. 100-106 ◽  
Author(s):  
Kenneth W. Van Treuren ◽  
Terrence Simon ◽  
Marc von Koller ◽  
Aaron R. Byerley ◽  
James W. Baughn ◽  
...  

With the new generation of gas turbine engines, low Reynolds number flows have become increasingly important. Designers must properly account for transition from laminar to turbulent flow and separation of the flow from the suction surface, which is strongly dependent upon transition. Of interest to industry are Reynolds numbers based upon suction surface length and flow exit velocity below 150,000 and as low as 25,000. In this paper, the extreme low end of this Reynolds number range is documented by way of pressure distributions, loss coefficients, and identification of separation zones. Reynolds numbers of 25,000 and 50,000 and with 1 percent and 8-9 percent turbulence intensity of the approach flow (free-stream turbulence intensity, FSTI) were investigated. At 25,000 Reynolds number and low FSTI, the suction surface displayed a strong and steady separation region. Raising the turbulence intensity resulted in a very unsteady separation region of nearly the same size on the suction surface. Vortex generators were added to the suction surface, but they appeared to do very little at this Reynolds number. At the higher Reynolds number of 50,000, the low-FSTI case was strongly separated on the downstream portion of the suction surface. The separation zone was eliminated when the turbulence level was increased to 8-9 percent. Vortex generators were added to the suction surface of the low-FSTI case. In this instance, the vortices were able to provide the mixing needed to re-establish flow attachment. This paper shows that massive separation at very low Reynolds numbers (25,000) is persistent, in spite of elevated FSTI and added vortices. However, at a higher Reynolds number, there is opportunity for flow reattachment either with elevated free-stream turbulence or with added vortices. This may be the first documentation of flow behavior at such low Reynolds numbers. Although it is undesirable to operate under these conditions, it is important to know what to expect and how performance may be improved if such conditions are unavoidable.


Author(s):  
Shuang Sun ◽  
Xingshuang Wu ◽  
Tianrong Tan ◽  
Canlin Zuo ◽  
Sirui Pan ◽  
...  

Abstract At low Reynolds numbers operating condition, the boundary layer of the high-lift low-pressure turbine (LPT) of aero-engines is prone to separate on the suction surface of the airfoil. The profile losses of the airfoil are largely governed by the size of the separation bubble and the transition process in the boundary layer. However, the wake-induced transition, the natural transition and the instability induced by the Klebanoff streaks complicate the transition process. The boundary layer on the suction surface of a high-lift LPT was investigated at Re = 50,000 with upstream wakes. The numerical simulation was performed with the CFX software using large eddy simulations (LES), and the experiment was performed on a linear cascade. In this study, the wake is divided into the wake center and the wake tail, the unsteady formation process of the streaks and the wall shear stress caused by the wake are analyzed. A new mechanism of generation and development of Klebanoff Streaks was presented to better understand the effect of the wake on the boundary layer. Moreover, it was found that after entering the blade passage, the wake center does not contact the blade but causes the wall shear stress of the front part on the suction surface to increase. However, it is not possible to form strong Klebanoff streaks at the leading edge of the blade by shear sheltering effect. Only the wake tail can form Klebanoff streaks when it contacts the blade.


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