Will stringent total nitrogen wastewater treatment plant discharge regulations achieve stream water quality goals?

2012 ◽  
Vol 14 (11) ◽  
pp. 2921 ◽  
Author(s):  
Ji-Hee Son ◽  
Kenneth H. Carlson
1992 ◽  
Vol 25 (4-5) ◽  
pp. 203-209 ◽  
Author(s):  
R. Kayser ◽  
G. Stobbe ◽  
M. Werner

At Wolfsburg for a load of 100,000 p.e., the step-feed activated sludge process for nitrogen removal is successfully in operation. Due to the high denitrification potential (BOD:TKN = 5:1) the effluent total nitrogen content can be kept below 10 mg l−1 N; furthermore by some enhanced biological phosphate removal about 80% phosphorus may be removed without any chemicals.


2010 ◽  
Vol 61 (9) ◽  
pp. 2259-2266 ◽  
Author(s):  
Styliani Kantartzi ◽  
Paraschos Melidis ◽  
Alexander Aivasidis

In the present study, a laboratory scale system, consisting of a primary settling tank, a continuous stirred tank reactor and a clarifier were constructed and operated, using wastewater from the municipal wastewater treatment plant in Xanthi, Greece. The system operated under intermittent aeration in aerobic/anoxic conditions and feeding of the wastewater once in every cycle. The unit was inoculated with sludge, which originated from the recirculation stream of the local wastewater treatment plant. The wastewater was processed with hydraulic retention time (HRT) of 12 h, in which various experimental states were studied regarding the combination of aerobic and anoxic intervals. The wastewater was fed in limited time once in every cycle of aerobic/anoxic conditions at the beginning of the anoxic period. The two states that exhibited highest performance in nitrification and total nitrogen removal were, then, repeated with HRT of 10 h. The results show that, regarding the nitrification stage and the organic load removal, the intermittent system achieved optimum efficiency, with an overall removal of biological oxygen demand (BOD5) and ammonium nitrogen in the range of 93–96% and 91–95% respectively. As far as the total nitrogen removal is concerned, and if the stage of the denitrification is taken into account, the performance of the intermittent system surpassed other methods, as it is shown by the total Kjeldahl nitrogen (TKN) removal efficiency of 85–87%. These operating conditions suppressed the growth of filamentous organisms, a fact reflected at the SVI values, which were lower than 150 ml/g.


2010 ◽  
Vol 61 (10) ◽  
pp. 2645-2652 ◽  
Author(s):  
S. Heusch ◽  
B. Kamradt ◽  
M. Ostrowski

In the federal state of Hesse in Germany the application of an integrated software modelling framework is becoming part of the planning process to attain legal approval for the operation of combined sewer systems. The software allows for parallel simulation of flow and water quality routing in the sewer system and in receiving rivers. It combines existing pollution load model approaches with a simplified version of the River Water Quality Model No. 1 (RWQM1). Comprehensive simulation of the wastewater treatment plant (WWTP) is not considered yet. The paper analyses alternatives for the implementation of a WWTP module to model activated sludge plants. For both primary and secondary clarifiers as well as for the activated sludge process concepts for the integration into the existing software framework were developed. The activated sludge concept which uses a linearized version of the well known ASM1 model is presented in detail.


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