Emission Rates of Regulated Pollutants from Current Technology Heavy-Duty Diesel and Natural Gas Goods Movement Vehicles

2015 ◽  
Vol 49 (8) ◽  
pp. 5236-5244 ◽  
Author(s):  
Arvind Thiruvengadam ◽  
Marc C. Besch ◽  
Pragalath Thiruvengadam ◽  
Saroj Pradhan ◽  
Daniel Carder ◽  
...  
Author(s):  
Jinlong Liu ◽  
Cosmin E. Dumitrescu

Increased utilization of natural-gas (NG) in the transportation sector can decrease the use of petroleum-based fuels and reduce greenhouse-gas emissions. Heavy-duty diesel engines retrofitted to NG spark ignition (SI) can achieve higher efficiencies and low NOx, CO, and HC emissions when operated under lean-burn conditions. To investigate the SI lean-burn combustion phenomena in a bowl-in-piston combustion chamber, a conventional heavy-duty direct-injection CI engine was converted to SI operation by replacing the fuel injector with a spark plug and by fumigating NG in the intake manifold. Steady-state engine experiments and numerical simulations were performed at several operating conditions that changed spark timing, engine speed, and mixture equivalence ratio. Results suggested a two-zone NG combustion inside the diesel-like combustion chamber. More frequent and significant late burn (including double-peak heat release rate) was observed for advanced spark timing. This was due to the chamber geometry affecting the local flame speed, which resulted in a faster and thicker flame in the bowl but a slower and thinner flame in the squish volume. Good combustion stability (COVIMEP < 3 %), moderate rate of pressure rise, and lack of knocking showed promise for heavy-duty CI engines converted to NG SI operation.


Author(s):  
Jinlong Liu ◽  
Cosmin Emil Dumitrescu

Increased utilization of natural gas (NG) in the transportation sector can decrease the use of petroleum-based fuels and reduced greenhouse gas emissions. Heavy-duty diesel engines retrofitted to NG spark ignition (SI) can achieve higher efficiencies and low NOX, CO, and hydrocarbon (HC) emissions when operated under lean-burn conditions. To investigate the SI lean-burn combustion phenomena in a bowl-in-piston combustion chamber, a conventional heavy-duty direct-injection CI engine was converted to SI operation by replacing the fuel injector with a spark plug and by fumigating NG in the intake manifold. Steady-state engine experiments and numerical simulations were performed at several operating conditions that changed spark timing (ST), engine speed, and mixture equivalence ratio. Results suggested a two-zone NG combustion inside the diesel-like combustion chamber. More frequent and significant late-burn (including double-peak heat release rate) was observed for advanced ST. This was due to the chamber geometry affecting the local flame speed, which resulted in a faster and thicker flame in the bowl but a slower and thinner flame in the squish volume. Good combustion stability (COVIMEP < 3%), moderate rate of pressure-rise, and lack of knocking showed promise for heavy-duty CI engines converted to NG SI operation.


Author(s):  
Jinlong Liu ◽  
Christopher Ulishney ◽  
Cosmin E. Dumitrescu

Abstract Converting existing compression ignition (CI) engines to spark ignition (SI) operation can increase the use of natural gas (NG) in heavy-duty engine applications and reduce the reliance on petroleum fuels. Gas fumigation upstream of the intake manifold and the addition of a spark plug in place of the diesel injector to initiate and control the combustion process is a convenient approach for converting existing diesel engines to dedicated NG operation. Stoichiometric operation and a three-way catalytic converter can help the engine to comply with increasingly strict emission regulations. However, as the CI-to-SI conversion usually maintains the conventional geometry of a CI engine (i.e., maintains the flat cylinder head and the bowl-in piston), the goal of this study was to observe some of the effects that the diesel conversion to stoichiometric NG SI operation will have on the engine’s performance and emissions. Dynamometer tests were performed at a constant engine speed at 1300 rpm but various spark timings. The experimental results for a net indicated mean effective pressure ∼ 6.7 bar showed that ignition timing did not affect the end of combustion due to the slow-burn inside the squish. Moreover, the less-optimal conditions inside the squish led to increased carbon monoxide (CO) and unburned hydrocarbon (UHC) emissions. While the combustion event was stable with no signs of knocking at the medium load conditions investigated here, the results suggest that the engine control needs to optimize the mass fraction trapped inside the squish region for a higher efficiency and lower emissions.


2016 ◽  
Vol 2 (3) ◽  
pp. 156-172 ◽  
Author(s):  
David C. Quiros ◽  
Arvind Thiruvengadam ◽  
Saroj Pradhan ◽  
Marc Besch ◽  
Pragalath Thiruvengadam ◽  
...  

2002 ◽  
Author(s):  
James Harrington ◽  
Sandeep Munshi ◽  
Costi Nedelcu ◽  
Patric Ouellette ◽  
Jeff Thompson ◽  
...  

Sign in / Sign up

Export Citation Format

Share Document